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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 492434 |
| Time | |
| Date | 200011 |
| Day | Mon |
| Local Time Of Day | 0601 To 1200 |
| Place | |
| Locale Reference | airport : fll.airport |
| State Reference | FL |
| Altitude | agl single value : 0 |
| Environment | |
| Flight Conditions | VMC |
| Light | Daylight |
| Aircraft 1 | |
| Controlling Facilities | tower : fll.tower |
| Operator | common carrier : air carrier |
| Make Model Name | B757-200 |
| Operating Under FAR Part | Part 121 |
| Flight Phase | ground : takeoff roll |
| Flight Plan | IFR |
| Person 1 | |
| Affiliation | company : air carrier |
| Function | flight crew : first officer |
| Qualification | pilot : atp pilot : commercial |
| Experience | flight time last 90 days : 160 flight time total : 3700 flight time type : 1540 |
| ASRS Report | 492434 |
| Person 2 | |
| Affiliation | company : air carrier |
| Function | flight crew : captain oversight : pic |
| Experience | flight time last 90 days : 150 flight time total : 15000 flight time type : 2000 |
| Events | |
| Anomaly | aircraft equipment problem : critical other anomaly other |
| Independent Detector | aircraft equipment other aircraft equipment : #1 engine indications other flight crewa other flight crewb |
| Resolutory Action | flight crew : rejected takeoff |
| Consequence | other other |
| Supplementary | |
| Problem Areas | Aircraft Flight Crew Human Performance |
| Primary Problem | Aircraft |
Narrative:
Captain applied power for takeoff. As power reached takeoff setting, after autothrottles were selected, we heard a loud bang and felt the aircraft shudder. We were just beginning the takeoff roll and I estimate our speed at 5-10 KTS. Captain initiated abort. We experienced a minor amount of smoke in the cockpit which quickly dissipated. The aircraft had initially veered left, so we just continued toward a taxiway and cleared the runway. We shut the left engine down as we were taxiing clear. Maintenance later showed us several pieces of metal, some 3-4 inches long, which they found in the engine cowl. There was also a layer of metal pieces in the engine exhaust area. All indications prior to the bang were normal, and the engines had warmed up for at least 5 mins prior to runup for takeoff. Callback conversation with reporter revealed the following information: the reporter stated the airplane was a B757-200 with P&west 4037 engines and the maintenance report indicated a failed high pressure turbine blade.
Original NASA ASRS Text
Title: A B757-200 REJECTED TKOF AT 10 KTS DUE #1 ENG LOUD BANG AND SHUDDER CAUSED BY A HIGH PRESSURE TURBINE BLADE FAILURE.
Narrative: CAPT APPLIED PWR FOR TKOF. AS PWR REACHED TKOF SETTING, AFTER AUTOTHROTTLES WERE SELECTED, WE HEARD A LOUD BANG AND FELT THE ACFT SHUDDER. WE WERE JUST BEGINNING THE TKOF ROLL AND I ESTIMATE OUR SPD AT 5-10 KTS. CAPT INITIATED ABORT. WE EXPERIENCED A MINOR AMOUNT OF SMOKE IN THE COCKPIT WHICH QUICKLY DISSIPATED. THE ACFT HAD INITIALLY VEERED L, SO WE JUST CONTINUED TOWARD A TXWY AND CLRED THE RWY. WE SHUT THE L ENG DOWN AS WE WERE TAXIING CLR. MAINT LATER SHOWED US SEVERAL PIECES OF METAL, SOME 3-4 INCHES LONG, WHICH THEY FOUND IN THE ENG COWL. THERE WAS ALSO A LAYER OF METAL PIECES IN THE ENG EXHAUST AREA. ALL INDICATIONS PRIOR TO THE BANG WERE NORMAL, AND THE ENGS HAD WARMED UP FOR AT LEAST 5 MINS PRIOR TO RUNUP FOR TKOF. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE AIRPLANE WAS A B757-200 WITH P&W 4037 ENGS AND THE MAINT RPT INDICATED A FAILED HIGH PRESSURE TURBINE BLADE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.