![]() |
37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
| Attributes | |
| ACN | 400698 |
| Time | |
| Date | 199804 |
| Day | Thu |
| Local Time Of Day | 1201 To 1800 |
| Place | |
| Locale Reference | airport : cgx |
| State Reference | IL |
| Altitude | agl bound lower : 0 agl bound upper : 500 |
| Environment | |
| Flight Conditions | VMC |
| Light | Daylight |
| Aircraft 1 | |
| Controlling Facilities | tracon : ord tower : cgx tower : stl |
| Operator | general aviation : personal |
| Make Model Name | Chancellor 414A & C414 |
| Operating Under FAR Part | Part 91 |
| Flight Phase | descent : approach landing other |
| Route In Use | approach : visual enroute : on vectors |
| Flight Plan | IFR |
| Person 1 | |
| Affiliation | Other |
| Function | flight crew : single pilot |
| Qualification | pilot : atp |
| Experience | flight time last 90 days : 120 flight time total : 3800 flight time type : 75 |
| ASRS Report | 400698 |
| Person 2 | |
| Affiliation | government : faa |
| Function | controller : approach |
| Qualification | controller : radar |
| Events | |
| Anomaly | aircraft equipment problem : critical incursion : landing without clearance non adherence : far non adherence : clearance other anomaly other |
| Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
| Resolutory Action | none taken : detected after the fact none taken : insufficient time |
| Consequence | Other |
| Supplementary | |
| Primary Problem | Aircraft |
| Air Traffic Incident | Pilot Deviation other |
Narrative:
On a visual approach into cgx, I was being vectored by chicago approach. The left engine started running rough so I tried adjusting the mixture and then turned the boost pump from 'low' to 'high.' when I did that, I was at about 200 ft AGL and the left engine quit. I was close enough to the runway to land safely and didn't have time for a restart. I didn't get or didn't hear the handoff from approach to tower and landed without a landing clearance.
Original NASA ASRS Text
Title: A C414 PLT LANDS WITHOUT CLRNC AT CGX WHEN HE IS DISTRACTED BY AN ENG FAILURE ON SHORT FINAL.
Narrative: ON A VISUAL APCH INTO CGX, I WAS BEING VECTORED BY CHICAGO APCH. THE L ENG STARTED RUNNING ROUGH SO I TRIED ADJUSTING THE MIXTURE AND THEN TURNED THE BOOST PUMP FROM 'LOW' TO 'HIGH.' WHEN I DID THAT, I WAS AT ABOUT 200 FT AGL AND THE L ENG QUIT. I WAS CLOSE ENOUGH TO THE RWY TO LAND SAFELY AND DIDN'T HAVE TIME FOR A RESTART. I DIDN'T GET OR DIDN'T HEAR THE HDOF FROM APCH TO TWR AND LANDED WITHOUT A LNDG CLRNC.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.