Narrative:

Autoplt attempted an uncommanded nose up at 7000 ft MSL approximately 10 DME northeast of dfw on modified base in 250 degree turn. Approximately 210 KTS idle power descent control column moved rapidly back within 1 to 3 inches back of full aft. The column came back so fast stick shaker activated and the aircraft shuddered approximately 1 second before the captain and myself simultaneously disconnected autoplt and pushed from approximately 20 degree nose up. Callback conversation with reporter revealed the following information: the reporter said the cause of the autoplt to pitch up was a short in the wiring to a 'flap logic' that occurs when the flaps are moved to the flaps 1 position. When the flaps were put in the #1 position, the nose pitched up to about 20 degrees so abruptly that the stick shaker actuated. Both pilots grabbed the wheel simultaneously, disconnected the autoplt, and pushed. There was a little less than the normal 1 positive G but no negative G's as they pushed. They also had a little bank which they rolled out of as they were in a left turn. There was no change in throttle position. He said that he learned about the 'flap logic' wire being 'frayed' from a conference call that occurred with the NTSB, NASA, FAA, company and union.

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Original NASA ASRS Text

Title: FLC EXPERIENCED AN AUTOPLT PITCH UP AND STICK SHAKER.

Narrative: AUTOPLT ATTEMPTED AN UNCOMMANDED NOSE UP AT 7000 FT MSL APPROX 10 DME NE OF DFW ON MODIFIED BASE IN 250 DEG TURN. APPROX 210 KTS IDLE PWR DSCNT CTL COLUMN MOVED RAPIDLY BACK WITHIN 1 TO 3 INCHES BACK OF FULL AFT. THE COLUMN CAME BACK SO FAST STICK SHAKER ACTIVATED AND THE ACFT SHUDDERED APPROX 1 SECOND BEFORE THE CAPT AND MYSELF SIMULTANEOUSLY DISCONNECTED AUTOPLT AND PUSHED FROM APPROX 20 DEG NOSE UP. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR SAID THE CAUSE OF THE AUTOPLT TO PITCH UP WAS A SHORT IN THE WIRING TO A 'FLAP LOGIC' THAT OCCURS WHEN THE FLAPS ARE MOVED TO THE FLAPS 1 POS. WHEN THE FLAPS WERE PUT IN THE #1 POS, THE NOSE PITCHED UP TO ABOUT 20 DEGS SO ABRUPTLY THAT THE STICK SHAKER ACTUATED. BOTH PLTS GRABBED THE WHEEL SIMULTANEOUSLY, DISCONNECTED THE AUTOPLT, AND PUSHED. THERE WAS A LITTLE LESS THAN THE NORMAL 1 POSITIVE G BUT NO NEGATIVE G'S AS THEY PUSHED. THEY ALSO HAD A LITTLE BANK WHICH THEY ROLLED OUT OF AS THEY WERE IN A L TURN. THERE WAS NO CHANGE IN THROTTLE POS. HE SAID THAT HE LEARNED ABOUT THE 'FLAP LOGIC' WIRE BEING 'FRAYED' FROM A CONFERENCE CALL THAT OCCURRED WITH THE NTSB, NASA, FAA, COMPANY AND UNION.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.