Narrative:

After gear retracted, captain's lower CRT went blank. After about 5 seconds, the screen reilluminated. A map shift occurred, showing an incorrect position for our departure fix. Las departure gave us heading for our RNAV fix. The navigation system reset in about 2 mins. The flight continued to dfw without incident. Maintenance in dfw detected large amounts of dust accumulation on the CRT connectors. The connectors were cleaned and the aircraft returned to las without incident. Supplemental information from acn 616854: I diverted my attention to the captain's problem instead of helping him navigation to our fix via heading select or calling departure for a radar vector. Maintenance detected large accumulations of dust on CRT connectors and near cooling fans which most likely lead to an overheated CRT and subsequent shutdown.

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Original NASA ASRS Text

Title: A B757-200 BTWN 400 FT AND 1500 FT, CAPT'S LOWER EHSI DISPLAY WENT BLANK. RETURNED IN 5 SECONDS, BUT MAP SHIFT OCCURRED SHOWING INCORRECT POS.

Narrative: AFTER GEAR RETRACTED, CAPT'S LOWER CRT WENT BLANK. AFTER ABOUT 5 SECONDS, THE SCREEN REILLUMINATED. A MAP SHIFT OCCURRED, SHOWING AN INCORRECT POS FOR OUR DEP FIX. LAS DEP GAVE US HDG FOR OUR RNAV FIX. THE NAV SYS RESET IN ABOUT 2 MINS. THE FLT CONTINUED TO DFW WITHOUT INCIDENT. MAINT IN DFW DETECTED LARGE AMOUNTS OF DUST ACCUMULATION ON THE CRT CONNECTORS. THE CONNECTORS WERE CLEANED AND THE ACFT RETURNED TO LAS WITHOUT INCIDENT. SUPPLEMENTAL INFO FROM ACN 616854: I DIVERTED MY ATTN TO THE CAPT'S PROB INSTEAD OF HELPING HIM NAV TO OUR FIX VIA HDG SELECT OR CALLING DEP FOR A RADAR VECTOR. MAINT DETECTED LARGE ACCUMULATIONS OF DUST ON CRT CONNECTORS AND NEAR COOLING FANS WHICH MOST LIKELY LEAD TO AN OVERHEATED CRT AND SUBSEQUENT SHUTDOWN.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.