Narrative:

Picked up from previous shift. Previous shift turned over they had found a leak at the outboard torque tube drive shaft at the inboard flap transmission. Previous shift had already removed drive shaft and replaced the o-ring. The assembly was reinstalled and failed a static leak check. I proceeded to remove the assembly and found the o-ring cut. I referenced the aircraft ipc and located the manufacturer's part number for the o-ring. Installed new o-ring. Reinstalled drive shaft assembly. Svced transmission. Transmission passed the static leak check and operational leak check. Aircraft was returned to service.

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Original NASA ASRS Text

Title: A B727-200 WAS DISPATCHED IN NON COMPLIANCE WITH AN UNAUTH REPAIR ACCOMPLISHED TO THE INBOARD FLAP TRANSMISSION.

Narrative: PICKED UP FROM PREVIOUS SHIFT. PREVIOUS SHIFT TURNED OVER THEY HAD FOUND A LEAK AT THE OUTBOARD TORQUE TUBE DRIVE SHAFT AT THE INBOARD FLAP TRANSMISSION. PREVIOUS SHIFT HAD ALREADY REMOVED DRIVE SHAFT AND REPLACED THE O-RING. THE ASSEMBLY WAS REINSTALLED AND FAILED A STATIC LEAK CHK. I PROCEEDED TO REMOVE THE ASSEMBLY AND FOUND THE O-RING CUT. I REFED THE ACFT IPC AND LOCATED THE MANUFACTURER'S PART NUMBER FOR THE O-RING. INSTALLED NEW O-RING. REINSTALLED DRIVE SHAFT ASSEMBLY. SVCED TRANSMISSION. TRANSMISSION PASSED THE STATIC LEAK CHK AND OPERATIONAL LEAK CHK. ACFT WAS RETURNED TO SVC.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.