Narrative:

On the date in question, a normal departure was made from day en route to sjc. At approximately XA00 PST. It was observed that the #2 engine oil quantity was slowly decreasing. All other engine indications were nominal. Company maintenance control was advised via company radio of the impending problem. At approximately XA58 PST with the engine oil quantity indicating about one quarter gallon, the engine oil pressure began to fluctuate and the in-flight engine shutdown checklist was accomplished for the #2 engine. WX at our destination and alternate was above basic VFR with rain and light winds. There were no other mechanical problems with the aircraft and as PIC I decided it would be as safe to proceed to sjc as to land at the nearest suitable airport (las). ZOA was advised of the engine shutdown and of our intention to proceed to sjc. An emergency was not declared and no additional assistance was requested at destination. A normal approach and landing was subsequently accomplished at sjc at XB58 PST. A captain's irregularity report of the above incident was submitted to the director of operations in accordance with the company general operation manual. A copy of the report is to be forwarded to the FAA. Cause of the oil leak was determined to be the installation of an incorrectly sized o-ring in an engine oil return line. The ring ruptured allowing the oil leak.

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Original NASA ASRS Text

Title: AN LGT ACFT SHUTS DOWN AN ENG W OF LAS AND CONTINUES ON TO SJC. ENG SHUTDOWN BECAUSE OF OIL LOSS.

Narrative: ON THE DATE IN QUESTION, A NORMAL DEP WAS MADE FROM DAY ENRTE TO SJC. AT APPROX XA00 PST. IT WAS OBSERVED THAT THE #2 ENG OIL QUANTITY WAS SLOWLY DECREASING. ALL OTHER ENG INDICATIONS WERE NOMINAL. COMPANY MAINT CTL WAS ADVISED VIA COMPANY RADIO OF THE IMPENDING PROB. AT APPROX XA58 PST WITH THE ENG OIL QUANTITY INDICATING ABOUT ONE QUARTER GALLON, THE ENG OIL PRESSURE BEGAN TO FLUCTUATE AND THE INFLT ENG SHUTDOWN CHKLIST WAS ACCOMPLISHED FOR THE #2 ENG. WX AT OUR DEST AND ALTERNATE WAS ABOVE BASIC VFR WITH RAIN AND LIGHT WINDS. THERE WERE NO OTHER MECHANICAL PROBS WITH THE ACFT AND AS PIC I DECIDED IT WOULD BE AS SAFE TO PROCEED TO SJC AS TO LAND AT THE NEAREST SUITABLE ARPT (LAS). ZOA WAS ADVISED OF THE ENG SHUTDOWN AND OF OUR INTENTION TO PROCEED TO SJC. AN EMER WAS NOT DECLARED AND NO ADDITIONAL ASSISTANCE WAS REQUESTED AT DEST. A NORMAL APCH AND LNDG WAS SUBSEQUENTLY ACCOMPLISHED AT SJC AT XB58 PST. A CAPT'S IRREGULARITY RPT OF THE ABOVE INCIDENT WAS SUBMITTED TO THE DIRECTOR OF OPS IN ACCORDANCE WITH THE COMPANY GENERAL OP MANUAL. A COPY OF THE RPT IS TO BE FORWARDED TO THE FAA. CAUSE OF THE OIL LEAK WAS DETERMINED TO BE THE INSTALLATION OF AN INCORRECTLY SIZED O-RING IN AN ENG OIL RETURN LINE. THE RING RUPTURED ALLOWING THE OIL LEAK.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.