Narrative:

After takeoff between 400-1000 ft AGL, smoke alarm in forward lavatory went off, cabin filled with smoke. Declared emergency and returned to atl, smoke dissipated on the ground, elected not to evacuate/evacuation, taxied to gate. Callback conversation with reporter revealed the following information: this reporter states that the forward lavatory smoke alarm sounded just after rotation in the boeing 737-200. The cabin crew simultaneously, initiated contact through the interphone. The reporter then, delegated the flying to the first officer, to meet the emergency. Apparently, the cabin crewmember was panicked, and time was lost in the exchange of cabin crewmembers on the interphone. The reporter directed the flight attendant to search the receptacles, and galleys, as the aircraft returned to land. On approach, the smoke dissipated. The problem, later, was thought to have been caused by oil on the air conditioning pack fan, which had been changed during the night preceding the flight. The takeoff maximum power brought maximum heat to the components, which caused excessive smoke to enter through the air conditioning ducts in the cabin. The smoke/smell was not obvious to the flight deck crew because the air conditioning source for the eyeball vents in the cockpit, is separate. There were no injuries -- the passenger were deplaned normally, at the gate.

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Original NASA ASRS Text

Title: AFTER A FLC'S DECLARATION OF AN EMER, A SMOKE FILLED ACFT RETURNED TO LAND.

Narrative: AFTER TKOF BTWN 400-1000 FT AGL, SMOKE ALARM IN FORWARD LAVATORY WENT OFF, CABIN FILLED WITH SMOKE. DECLARED EMER AND RETURNED TO ATL, SMOKE DISSIPATED ON THE GND, ELECTED NOT TO EVAC, TAXIED TO GATE. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THIS RPTR STATES THAT THE FORWARD LAVATORY SMOKE ALARM SOUNDED JUST AFTER ROTATION IN THE BOEING 737-200. THE CABIN CREW SIMULTANEOUSLY, INITIATED CONTACT THROUGH THE INTERPHONE. THE RPTR THEN, DELEGATED THE FLYING TO THE FO, TO MEET THE EMER. APPARENTLY, THE CABIN CREWMEMBER WAS PANICKED, AND TIME WAS LOST IN THE EXCHANGE OF CABIN CREWMEMBERS ON THE INTERPHONE. THE RPTR DIRECTED THE FLT ATTENDANT TO SEARCH THE RECEPTACLES, AND GALLEYS, AS THE ACFT RETURNED TO LAND. ON APCH, THE SMOKE DISSIPATED. THE PROB, LATER, WAS THOUGHT TO HAVE BEEN CAUSED BY OIL ON THE AIR CONDITIONING PACK FAN, WHICH HAD BEEN CHANGED DURING THE NIGHT PRECEDING THE FLT. THE TKOF MAX PWR BROUGHT MAX HEAT TO THE COMPONENTS, WHICH CAUSED EXCESSIVE SMOKE TO ENTER THROUGH THE AIR CONDITIONING DUCTS IN THE CABIN. THE SMOKE/SMELL WAS NOT OBVIOUS TO THE FLT DECK CREW BECAUSE THE AIR CONDITIONING SOURCE FOR THE EYEBALL VENTS IN THE COCKPIT, IS SEPARATE. THERE WERE NO INJURIES -- THE PAX WERE DEPLANED NORMALLY, AT THE GATE.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.