Narrative:

Aircraft X came in with #2 engine; system #1 ignition on MEL. After pushback the #2 engine would not start. We called for the control center to order us 2 exciter units; which I installed. The operation check failed. At this point it was the end of our shift. In order to avoid paperwork issues with next shift; I signed off the log page as replaced units test fails and opened a new log page. Today I found out in (computer system) that next shift had to replace both exciter units again due to (incorrect) effectivity; which fixed the problem. Next shift found the problem and it was corrected before flight. I should have verified the effectivity; not assume the (controller) ordering the parts would do so.

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Original NASA ASRS Text

Title: A B757-300 ACFT #2 ENGINE (RB-211) REQUIRED BOTH IGNITER EXCITERS REPLACED DUE TO FAILED START. OPS TESTS FAILED. USED INCORRECT EFFECTIVITY.

Narrative: ACFT X CAME IN WITH #2 ENG; SYS #1 IGNITION ON MEL. AFTER PUSHBACK THE #2 ENG WOULD NOT START. WE CALLED FOR THE CTL CTR TO ORDER US 2 EXCITER UNITS; WHICH I INSTALLED. THE OP CHK FAILED. AT THIS POINT IT WAS THE END OF OUR SHIFT. IN ORDER TO AVOID PAPERWORK ISSUES WITH NEXT SHIFT; I SIGNED OFF THE LOG PAGE AS REPLACED UNITS TEST FAILS AND OPENED A NEW LOG PAGE. TODAY I FOUND OUT IN (COMPUTER SYS) THAT NEXT SHIFT HAD TO REPLACE BOTH EXCITER UNITS AGAIN DUE TO (INCORRECT) EFFECTIVITY; WHICH FIXED THE PROB. NEXT SHIFT FOUND THE PROB AND IT WAS CORRECTED BEFORE FLT. I SHOULD HAVE VERIFIED THE EFFECTIVITY; NOT ASSUME THE (CTLR) ORDERING THE PARTS WOULD DO SO.

Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.