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| Attributes | |
| ACN | 582630 |
| Time | |
| Date | 200305 |
| Day | Mon |
| Local Time Of Day | 1201 To 1800 |
| Place | |
| Locale Reference | airport : ahn.airport |
| State Reference | GA |
| Altitude | msl bound lower : 2000 msl bound upper : 3000 |
| Environment | |
| Flight Conditions | VMC |
| Light | Daylight |
| Aircraft 1 | |
| Controlling Facilities | tower : ahn.tower |
| Operator | general aviation : personal |
| Make Model Name | Cessna 152 |
| Operating Under FAR Part | Part 91 |
| Flight Phase | climbout : intermediate altitude |
| Flight Plan | None |
| Person 1 | |
| Affiliation | other |
| Function | flight crew : single pilot |
| Qualification | pilot : instrument pilot : private |
| Experience | flight time last 90 days : 3 flight time total : 220 flight time type : 60 |
| ASRS Report | 582630 |
| Person 2 | |
| Affiliation | government : faa |
| Function | controller : local |
| Events | |
| Anomaly | aircraft equipment problem : less severe |
| Independent Detector | other flight crewa |
| Resolutory Action | none taken : detected after the fact |
| Consequence | faa : reviewed incident with flight crew other |
| Supplementary | |
| Problem Areas | Flight Crew Human Performance Aircraft |
| Primary Problem | Aircraft |
Narrative:
After takeoff, microphone became stuck. I perceived an intercom failure and after a few mins of trying to rectify, I gave up on fixing while on flight. After approximately 30 mins, I contacted tower for a landing clearance, when I was informed I had a stuck microphone for almost 30 mins. The button had been physically stuck, as I had removed my hands from the controls on several occasions to let passenger steer the plane. In the future, I will always make sure to double-check the microphone button on any radio failures. I have also referred plane to maintenance, as it was a flight school aircraft.
Original NASA ASRS Text
Title: C152 DEP FROM AHN EXPERIENCED STUCK MIKE FOR APPROX 30 MINS.
Narrative: AFTER TKOF, MIKE BECAME STUCK. I PERCEIVED AN INTERCOM FAILURE AND AFTER A FEW MINS OF TRYING TO RECTIFY, I GAVE UP ON FIXING WHILE ON FLT. AFTER APPROX 30 MINS, I CONTACTED TWR FOR A LNDG CLRNC, WHEN I WAS INFORMED I HAD A STUCK MIKE FOR ALMOST 30 MINS. THE BUTTON HAD BEEN PHYSICALLY STUCK, AS I HAD REMOVED MY HANDS FROM THE CTLS ON SEVERAL OCCASIONS TO LET PAX STEER THE PLANE. IN THE FUTURE, I WILL ALWAYS MAKE SURE TO DOUBLE-CHK THE MIKE BUTTON ON ANY RADIO FAILURES. I HAVE ALSO REFERRED PLANE TO MAINT, AS IT WAS A FLT SCHOOL ACFT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.