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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 557754 |
| Time | |
| Date | 200208 |
| Day | Sat |
| Local Time Of Day | 1201 To 1800 |
| Place | |
| Locale Reference | airport : fdk.airport |
| State Reference | MD |
| Altitude | agl bound lower : 0 agl bound upper : 300 |
| Environment | |
| Flight Conditions | VMC |
| Light | Daylight |
| Aircraft 1 | |
| Operator | general aviation : personal |
| Make Model Name | Small Aircraft |
| Operating Under FAR Part | Part 91 |
| Flight Phase | climbout : takeoff cruise : level cruise : holding |
| Flight Plan | None |
| Aircraft 2 | |
| Operator | general aviation : personal |
| Make Model Name | Small Aircraft |
| Operating Under FAR Part | Part 91 |
| Flight Phase | cruise : level cruise : holding |
| Flight Plan | None |
| Person 1 | |
| Affiliation | other |
| Function | flight crew : single pilot |
| Qualification | pilot : instrument pilot : private |
| Experience | flight time last 90 days : 10 flight time total : 1750 flight time type : 250 |
| ASRS Report | 557754 |
| Person 2 | |
| Affiliation | other |
| Function | flight crew : single pilot |
| Events | |
| Anomaly | aircraft equipment problem : critical other anomaly other |
| Independent Detector | other flight crewa |
| Resolutory Action | flight crew : landed in emergency condition |
| Consequence | other other |
| Supplementary | |
| Problem Areas | Aircraft |
| Primary Problem | Aircraft |
Narrative:
We were in a race track pattern with all the l-baids at 300 ft, pt's and trainers at 500 ft, and faska trainers bt's, T6's at 700 ft during the airshow. Preflight briefing was completed. Taxi and run-up completed with no indications of rough engine seen. After making takeoff and 1 circuit around, the engine began to lose power and within 10 seconds quit. I made a dead stick landing back on runway 5 downwind. No damage to plane. Looks like oil pump failed or stuck valves.
Original NASA ASRS Text
Title: PLT OF A RACING T CRAFT L2M PERFORMS A FORCED EMER DOWNWIND LNDG DURING AN AIR RACE AT FDK, MD.
Narrative: WE WERE IN A RACE TRACK PATTERN WITH ALL THE L-BAIDS AT 300 FT, PT'S AND TRAINERS AT 500 FT, AND FASKA TRAINERS BT'S, T6'S AT 700 FT DURING THE AIRSHOW. PREFLT BRIEFING WAS COMPLETED. TAXI AND RUN-UP COMPLETED WITH NO INDICATIONS OF ROUGH ENG SEEN. AFTER MAKING TKOF AND 1 CIRCUIT AROUND, THE ENG BEGAN TO LOSE PWR AND WITHIN 10 SECONDS QUIT. I MADE A DEAD STICK LNDG BACK ON RWY 5 DOWNWIND. NO DAMAGE TO PLANE. LOOKS LIKE OIL PUMP FAILED OR STUCK VALVES.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.