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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 542822 |
| Time | |
| Date | 200203 |
| Day | Fri |
| Local Time Of Day | 0601 To 1200 |
| Place | |
| Locale Reference | airport : zzz.airport |
| State Reference | US |
| Altitude | agl single value : 0 |
| Environment | |
| Light | Daylight |
| Aircraft 1 | |
| Controlling Facilities | tower : lga.tower |
| Operator | common carrier : air carrier |
| Make Model Name | A310 |
| Operating Under FAR Part | Part 121 |
| Navigation In Use | other |
| Flight Phase | ground : maintenance |
| Flight Plan | IFR |
| Person 1 | |
| Affiliation | company : air carrier |
| Function | maintenance : technician |
| Qualification | technician : airframe technician : powerplant |
| ASRS Report | 542822 |
| Person 2 | |
| Affiliation | company : air carrier |
| Function | maintenance : technician |
| Qualification | technician : powerplant technician : airframe |
| ASRS Report | 542823 |
| Events | |
| Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance non adherence : far non adherence : published procedure |
| Independent Detector | aircraft equipment other aircraft equipment : engine press quantity indications other flight crewa other flight crewb |
| Resolutory Action | flight crew : diverted to another airport |
| Consequence | other other |
| Factors | |
| Maintenance | performance deficiency : installation performance deficiency : testing performance deficiency : inspection |
| Supplementary | |
| Problem Areas | Maintenance Human Performance Aircraft Environmental Factor |
| Primary Problem | Maintenance Human Performance |
Narrative:
Low pressure turbine cooling of manifold and oil lines were disconnected by another mechanic on 03/fri/02. I installed a low pressure turbine manifold and oil line on 03/xx/02 and wet motored on 03/mon/02 and found no leaks. Crew chief log on run-up noted oil leak. Checked engine over and found no evidence of oil or leaks on 03/thu/02. No discrepancy on leaking oil. Checked oil quantity and found to be good. Aircraft was dispatched to air carrier loading area at XA35 03/sat/02. No oil leaks found. Air interrupt on 03/sat/02 at approximately XA50.
Original NASA ASRS Text
Title: AN AIRBUS 310 SHORTLY AFTER TKOF RETURNED TO THE FIELD DUE TO LOSS OF OIL PRESSURE AND QUANTITY FROM LEAKING OIL SCAVENGE LINE.
Narrative: LOW PRESSURE TURBINE COOLING OF MANIFOLD AND OIL LINES WERE DISCONNECTED BY ANOTHER MECH ON 03/FRI/02. I INSTALLED A LOW PRESSURE TURBINE MANIFOLD AND OIL LINE ON 03/XX/02 AND WET MOTORED ON 03/MON/02 AND FOUND NO LEAKS. CREW CHIEF LOG ON RUN-UP NOTED OIL LEAK. CHKED ENG OVER AND FOUND NO EVIDENCE OF OIL OR LEAKS ON 03/THU/02. NO DISCREPANCY ON LEAKING OIL. CHKED OIL QUANTITY AND FOUND TO BE GOOD. ACFT WAS DISPATCHED TO ACR LOADING AREA AT XA35 03/SAT/02. NO OIL LEAKS FOUND. AIR INTERRUPT ON 03/SAT/02 AT APPROX XA50.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.