Narrative:

During a routine phase 2 and hot section on the right engine, a discrepancy was noted in the total time of the right engine. Prior to this date a change was made on the total time on this engine based on an entry made by an overhaul shop. The overhaul shop added 50.6 hours to the total time, based on the 50.6 hours of flight time put on the rental engine, not the overhauled engine. When the 50.6 hours was subtracted, it was found that we flew the aircraft 32.5 hours over the scheduled hot section. Upon consultation with pratt & whitney field representative, there should be no adverse effect.

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Original NASA ASRS Text

Title: A BEECH KING AIR 200 WAS FLOWN IN NON COMPLIANCE WITH A R ENG HOT SECTION INSPECTION OVERDUE BY 32 HRS CAUSED BY AN ERROR IN ENG OVERHAUL SHOP.

Narrative: DURING A ROUTINE PHASE 2 AND HOT SECTION ON THE R ENG, A DISCREPANCY WAS NOTED IN THE TOTAL TIME OF THE R ENG. PRIOR TO THIS DATE A CHANGE WAS MADE ON THE TOTAL TIME ON THIS ENG BASED ON AN ENTRY MADE BY AN OVERHAUL SHOP. THE OVERHAUL SHOP ADDED 50.6 HRS TO THE TOTAL TIME, BASED ON THE 50.6 HRS OF FLT TIME PUT ON THE RENTAL ENG, NOT THE OVERHAULED ENG. WHEN THE 50.6 HRS WAS SUBTRACTED, IT WAS FOUND THAT WE FLEW THE ACFT 32.5 HRS OVER THE SCHEDULED HOT SECTION. UPON CONSULTATION WITH PRATT & WHITNEY FIELD REPRESENTATIVE, THERE SHOULD BE NO ADVERSE EFFECT.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.