Narrative:

During leveloff at FL310, 275 KIAS, the power was reduced from climb EPR, 2.11 to cruse EPR, 1.86. #1 engine had a compressor stall. Abnormal procedures were accomplished, followed by normal engine operation. During engine inspection at msy we found an 18 inch piece of rubber which apparently came from the left leading edge device. The main point of this debrief is to document another problem shortly after a major inspection. I do not consider myself a test pilot. This was the 5TH flight since coming back from maintenance. These problems should have been discovered earlier by maintenance or during the flight test.

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Original NASA ASRS Text

Title: B727 CREW HAD A COMPRESSOR STALL IN #1 ENG. FOD FROM A DEICING BOOT ON L WING.

Narrative: DURING LEVELOFF AT FL310, 275 KIAS, THE PWR WAS REDUCED FROM CLB EPR, 2.11 TO CRUSE EPR, 1.86. #1 ENG HAD A COMPRESSOR STALL. ABNORMAL PROCS WERE ACCOMPLISHED, FOLLOWED BY NORMAL ENG OP. DURING ENG INSPECTION AT MSY WE FOUND AN 18 INCH PIECE OF RUBBER WHICH APPARENTLY CAME FROM THE L LEADING EDGE DEVICE. THE MAIN POINT OF THIS DEBRIEF IS TO DOCUMENT ANOTHER PROB SHORTLY AFTER A MAJOR INSPECTION. I DO NOT CONSIDER MYSELF A TEST PLT. THIS WAS THE 5TH FLT SINCE COMING BACK FROM MAINT. THESE PROBS SHOULD HAVE BEEN DISCOVERED EARLIER BY MAINT OR DURING THE FLT TEST.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.