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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 381085 |
| Time | |
| Date | 199709 |
| Day | Sat |
| Local Time Of Day | 0601 To 1200 |
| Place | |
| Locale Reference | atc facility : mia |
| State Reference | FL |
| Altitude | msl bound lower : 17000 msl bound upper : 17000 |
| Environment | |
| Flight Conditions | VMC |
| Light | Daylight |
| Aircraft 1 | |
| Operator | common carrier : air carrier |
| Make Model Name | B757 Undifferentiated or Other Model |
| Operating Under FAR Part | Part 121 |
| Navigation In Use | Other Other |
| Flight Phase | climbout : intermediate altitude |
| Route In Use | departure other departure sid : sid enroute airway : zma |
| Flight Plan | IFR |
| Person 1 | |
| Affiliation | company : air carrier |
| Function | flight crew : first officer |
| Qualification | pilot : atp |
| Experience | flight time last 90 days : 150 flight time total : 8000 flight time type : 85 |
| ASRS Report | 381085 |
| Person 2 | |
| Affiliation | company : air carrier |
| Function | flight crew : captain oversight : pic |
| Qualification | pilot : atp |
| Experience | flight time last 90 days : 120 flight time total : 10000 flight time type : 500 |
| ASRS Report | 381085 |
| Events | |
| Anomaly | aircraft equipment problem : critical other anomaly other |
| Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
| Resolutory Action | flight crew : declared emergency other |
| Consequence | Other |
| Supplementary | |
| Primary Problem | Aircraft |
Narrative:
The situation was decreasing oil quantity during climb out of miami international airport, with eventual complete loss of oil in the #2 engine. The engine was shut down and all applicable checklist completed. A return to miami was decided with a normal approach and landing (single engine). Maintenance advised that we had a bad blowout seal possibly a result from a replaced generator the night before. The captain did an outstanding job of CRM with first officer, flight attendants and passenger. We worked together well as a team. (Added note: the captain did have 2 quarts added to the #2 engine prior to departure.)
Original NASA ASRS Text
Title: FLC OF A B757 RETURNED TO LAND AFTER SHUTTING DOWN 1 ENG DUE TO LOSS OF OIL QUANTITY.
Narrative: THE SIT WAS DECREASING OIL QUANTITY DURING CLBOUT OF MIAMI INTL ARPT, WITH EVENTUAL COMPLETE LOSS OF OIL IN THE #2 ENG. THE ENG WAS SHUT DOWN AND ALL APPLICABLE CHKLIST COMPLETED. A RETURN TO MIAMI WAS DECIDED WITH A NORMAL APCH AND LNDG (SINGLE ENG). MAINT ADVISED THAT WE HAD A BAD BLOWOUT SEAL POSSIBLY A RESULT FROM A REPLACED GENERATOR THE NIGHT BEFORE. THE CAPT DID AN OUTSTANDING JOB OF CRM WITH FO, FLT ATTENDANTS AND PAX. WE WORKED TOGETHER WELL AS A TEAM. (ADDED NOTE: THE CAPT DID HAVE 2 QUARTS ADDED TO THE #2 ENG PRIOR TO DEP.)
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.