![]() |
37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
| Attributes | |
| ACN | 224884 |
| Time | |
| Date | 199210 |
| Day | Thu |
| Local Time Of Day | 1801 To 2400 |
| Place | |
| Locale Reference | atc facility : ott |
| State Reference | MD |
| Altitude | msl bound lower : 13000 msl bound upper : 13000 |
| Environment | |
| Flight Conditions | Marginal |
| Light | Night |
| Aircraft 1 | |
| Operator | common carrier : air carrier |
| Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
| Flight Phase | cruise other |
| Route In Use | arrival other arrival star : star enroute airway : zdc |
| Flight Plan | IFR |
| Person 1 | |
| Affiliation | company : air carrier |
| Function | flight crew : captain oversight : pic |
| Qualification | pilot : flight engineer pilot : atp |
| Experience | flight time last 90 days : 230 flight time total : 12000 flight time type : 10000 |
| ASRS Report | 224884 |
| Person 2 | |
| Affiliation | company : air carrier |
| Function | flight crew : first officer |
| Qualification | pilot : atp |
| Experience | flight time last 90 days : 150 flight time total : 10000 flight time type : 4000 |
| ASRS Report | 224786 |
| Events | |
| Anomaly | other anomaly other |
| Independent Detector | other controllera other flight crewa |
| Resolutory Action | other |
| Consequence | faa : reviewed incident with flight crew |
| Supplementary | |
| Primary Problem | Flight Crew Human Performance |
| Air Traffic Incident | Pilot Deviation |
Narrative:
While on the ott 2 arrival to bwi at 13000 ft we realized its been awfully quiet and we should have been passed to approach. When checking with center and the radios it was apparent #1 communication had been inadvertently shut off while picking up the current ATIS at bwi. Once contact was re-established with center we were given a few turns and rapid descent then turned over to bwi approach. After landing a call was made to bwi tower and I was told there was no problem, we were treated as a norad and handled accordingly. Closer adherence to radio work could and would have prevented the entire episode! It was a 13 hour duty day and we were on our fifth of 6 approachs. Fatigue was a definite factor! Supplemental information from acn 224786: bad on my part, as should have made sure captain was listening to radio, should also have advised him I'd be off frequency for a min. Fatigue played a part as we were towards the end of 13 hour day.
Original NASA ASRS Text
Title: RADIOS OF CAPT NEVER TURNED ON, FO RADIO TURNED OFF WHILE RECEIVING ATIS. RECONTACTED ATC WHEN REALIZED.
Narrative: WHILE ON THE OTT 2 ARR TO BWI AT 13000 FT WE REALIZED ITS BEEN AWFULLY QUIET AND WE SHOULD HAVE BEEN PASSED TO APCH. WHEN CHKING WITH CTR AND THE RADIOS IT WAS APPARENT #1 COM HAD BEEN INADVERTENTLY SHUT OFF WHILE PICKING UP THE CURRENT ATIS AT BWI. ONCE CONTACT WAS RE-ESTABLISHED WITH CTR WE WERE GIVEN A FEW TURNS AND RAPID DSCNT THEN TURNED OVER TO BWI APCH. AFTER LNDG A CALL WAS MADE TO BWI TWR AND I WAS TOLD THERE WAS NO PROBLEM, WE WERE TREATED AS A NORAD AND HANDLED ACCORDINGLY. CLOSER ADHERENCE TO RADIO WORK COULD AND WOULD HAVE PREVENTED THE ENTIRE EPISODE! IT WAS A 13 HR DUTY DAY AND WE WERE ON OUR FIFTH OF 6 APCHS. FATIGUE WAS A DEFINITE FACTOR! SUPPLEMENTAL INFO FROM ACN 224786: BAD ON MY PART, AS SHOULD HAVE MADE SURE CAPT WAS LISTENING TO RADIO, SHOULD ALSO HAVE ADVISED HIM I'D BE OFF FREQ FOR A MIN. FATIGUE PLAYED A PART AS WE WERE TOWARDS THE END OF 13 HR DAY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.