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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 1394633 |
| Time | |
| Date | 201610 |
| Local Time Of Day | 1801-2400 |
| Place | |
| Locale Reference | ZZZ.Airport |
| State Reference | US |
| Environment | |
| Flight Conditions | VMC |
| Aircraft 1 | |
| Make Model Name | B737 Undifferentiated or Other Model |
| Operating Under FAR Part | Part 121 |
| Flight Phase | Climb |
| Flight Plan | IFR |
| Component | |
| Aircraft Component | Turbine Engine |
| Person 1 | |
| Function | Pilot Flying Captain |
| Qualification | Flight Crew Air Transport Pilot (ATP) |
| Experience | Flight Crew Last 90 Days 200 Flight Crew Total 20000 Flight Crew Type 1500 |
| Person 2 | |
| Function | First Officer Pilot Not Flying |
| Qualification | Flight Crew Air Transport Pilot (ATP) |
| Experience | Flight Crew Last 90 Days 143 Flight Crew Total 15750 Flight Crew Type 2500 |
| Events | |
| Anomaly | Aircraft Equipment Problem Less Severe Inflight Event / Encounter Bird / Animal |
Narrative:
Approximately 500 feet (after gear retraction but prior to flap retraction) jolt/yaw accompanied by bang similar to those experienced in simulator (associated with severe damage). I was hand flying (and focused on that) and by the time I looked at the engine instruments; all appeared normal. At the same time a strong burning smell was experienced. We quickly decided to return and not continue. We communicated with departure and stated our intentions. A few minutes after the odor started; it began to dissipate. ATC gave us a heading and assigned 9000 as an altitude. I engaged the autopilot (after the first officer reminded me it was available). The first officer ran the after takeoff checklist as well as set up the box for the return. I called the flight attendants and informed them of our situation. They informed me that they saw torching in the left engine when the bang occurred. The first officer and I concluded that we most likely ingested a bird into the left engine and that the engine had a compressor stall. I sent a message to dispatch informing them of our condition and intent to return. Dispatch requested the emergency equipment for us. The first officer and I discussed our landing overweight; and continued back for an uneventful landing (overweight).
Original NASA ASRS Text
Title: B737 flight crew reported a bird strike below 1;000 feet on departure which caused a momentary compressor stall before resuming normal operation. Flight returns to the departure airport for an overweight landing.
Narrative: Approximately 500 feet (after gear retraction but prior to flap retraction) jolt/yaw accompanied by bang similar to those experienced in simulator (associated with severe damage). I was hand flying (and focused on that) and by the time I looked at the engine instruments; all appeared normal. At the same time a strong burning smell was experienced. We quickly decided to return and not continue. We communicated with departure and stated our intentions. A few minutes after the odor started; it began to dissipate. ATC gave us a heading and assigned 9000 as an altitude. I engaged the autopilot (after the FO reminded me it was available). The FO ran the after takeoff checklist as well as set up the box for the return. I called the flight attendants and informed them of our situation. They informed me that they saw torching in the left engine when the bang occurred. The FO and I concluded that we most likely ingested a bird into the left engine and that the engine had a compressor stall. I sent a message to dispatch informing them of our condition and intent to return. Dispatch requested the emergency equipment for us. The FO and I discussed our landing overweight; and continued back for an uneventful landing (overweight).
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.