Narrative:

Flight las-pit. Takeoff roll began at approximately XX40 EST. At 80 KTS IAS I released the nose wheel steering. Power ok, roll ok. At approximately 100 KIAS rumbling and shaking began. Rejected takeoff procedures in effect. Rejected takeoff/autobrake, reverse ok. Very slight pull to the right. Stopped fairly centered on runway. Notified tower and taxied clear of runway with a slight wobble. No excessive power on taxiway noted aircraft listing to the right. Suspected right main gear tires blown. Notified tower, ground control, company, passenger and shut down engines. Excellent response from all ground personnel.

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Original NASA ASRS Text

Title: MLG ABORTED TKOF BECAUSE OF SEVERE VIBRATION.

Narrative: FLT LAS-PIT. TKOF ROLL BEGAN AT APPROX XX40 EST. AT 80 KTS IAS I RELEASED THE NOSE WHEEL STEERING. PWR OK, ROLL OK. AT APPROX 100 KIAS RUMBLING AND SHAKING BEGAN. REJECTED TKOF PROCS IN EFFECT. RTO/AUTOBRAKE, REVERSE OK. VERY SLIGHT PULL TO THE RIGHT. STOPPED FAIRLY CENTERED ON RWY. NOTIFIED TWR AND TAXIED CLR OF RWY WITH A SLIGHT WOBBLE. NO EXCESSIVE PWR ON TXWY NOTED ACFT LISTING TO THE RIGHT. SUSPECTED RIGHT MAIN GEAR TIRES BLOWN. NOTIFIED TWR, GND CTL, COMPANY, PAX AND SHUT DOWN ENGS. EXCELLENT RESPONSE FROM ALL GND PERSONNEL.

Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.