Narrative:

On departure from boston; just after wheels up; a sliding noise was heard followed by a thump. Some vibration was noted in the yoke followed by the flight attendants calling the cockpit to inform us of the vibration in the tail. The vibration continued and appeared to be getting worse. The flight crew requested permission to return to boston to have the vibration inspected by maintenance. The approach and landing were uneventful. Boston crash fire rescue equipment followed the aircraft to the gate. One of the possibilities for the vibration was a bird strike; but no bird strike was found after inspecting the aircraft. The aircraft was taken OTS for further inspection. An emergency was not declared; however; it was handled as an emergency by ATC. Callback conversation with reporter revealed the following information: the reporter stated that the vibrations started after rotation; with noise and vibrations in the control column and tail. The vibrations were increasing and the decision was made to return to the field. Landing was uneventful but on taxi in; got #2 engine filter clog light. Maintenance pulled the main oil screen and found it full of metal. The screen was replaced and the engine would not rotate when a start was attempted. Airplane was removed from service and the engine replaced. Supplemental information from acn 674914: we heard a thump; followed by a brief moan coming from somewhere aft of the cockpit.

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Original NASA ASRS Text

Title: AN MD80 FLT CREW; AFTER ROTATION; HEARD THUMP AND MOAN ALONG WITH VIBRATIONS IN TAIL AND CTL COLUMN. ALL ENG AND CTL INDICATIONS NORMAL. RETURNED TO FIELD. ON GND; #2 ENG OIL FILTER CLOG LIGHT ON.

Narrative: ON DEP FROM BOSTON; JUST AFTER WHEELS UP; A SLIDING NOISE WAS HEARD FOLLOWED BY A THUMP. SOME VIBRATION WAS NOTED IN THE YOKE FOLLOWED BY THE FLT ATTENDANTS CALLING THE COCKPIT TO INFORM US OF THE VIBRATION IN THE TAIL. THE VIBRATION CONTINUED AND APPEARED TO BE GETTING WORSE. THE FLT CREW REQUESTED PERMISSION TO RETURN TO BOSTON TO HAVE THE VIBRATION INSPECTED BY MAINT. THE APCH AND LNDG WERE UNEVENTFUL. BOSTON CFR FOLLOWED THE ACFT TO THE GATE. ONE OF THE POSSIBILITIES FOR THE VIBRATION WAS A BIRD STRIKE; BUT NO BIRD STRIKE WAS FOUND AFTER INSPECTING THE ACFT. THE ACFT WAS TAKEN OTS FOR FURTHER INSPECTION. AN EMER WAS NOT DECLARED; HOWEVER; IT WAS HANDLED AS AN EMER BY ATC. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THAT THE VIBRATIONS STARTED AFTER ROTATION; WITH NOISE AND VIBRATIONS IN THE CTL COLUMN AND TAIL. THE VIBRATIONS WERE INCREASING AND THE DECISION WAS MADE TO RETURN TO THE FIELD. LNDG WAS UNEVENTFUL BUT ON TAXI IN; GOT #2 ENG FILTER CLOG LIGHT. MAINT PULLED THE MAIN OIL SCREEN AND FOUND IT FULL OF METAL. THE SCREEN WAS REPLACED AND THE ENG WOULD NOT ROTATE WHEN A START WAS ATTEMPTED. AIRPLANE WAS REMOVED FROM SVC AND THE ENG REPLACED. SUPPLEMENTAL INFO FROM ACN 674914: WE HEARD A THUMP; FOLLOWED BY A BRIEF MOAN COMING FROM SOMEWHERE AFT OF THE COCKPIT.

Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.