Narrative:

After takeoff, landing gear would not come up. Landing gear lever would not go above 'off' position. Landing gear override trigger was pulled, gear still did not come up. Aircraft returned to okc. Checklist was run for the problem. Aircraft landed at okc, overweight landing at 116200 pounds. Supplemental information from acn 622306: aircraft was leveled off in VMC at 5000 ft MSL. Qrc checklist was run with no results. 'Trigger pull' was accomplished in accordance with the checklist. Both pilots attempted to 'trigger pull,' gear handle still would not go beyond 'off' position. Landed the aircraft uneventfully at okc approximately 2000 pounds overweight (116200 pounds).

Google
 

Original NASA ASRS Text

Title: B737 CREW WAS UNABLE TO RETRACT THE LNDG GEAR AFTER TKOF AT OKC.

Narrative: AFTER TKOF, LNDG GEAR WOULD NOT COME UP. LNDG GEAR LEVER WOULD NOT GO ABOVE 'OFF' POS. LNDG GEAR OVERRIDE TRIGGER WAS PULLED, GEAR STILL DID NOT COME UP. ACFT RETURNED TO OKC. CHKLIST WAS RUN FOR THE PROB. ACFT LANDED AT OKC, OVERWT LNDG AT 116200 LBS. SUPPLEMENTAL INFO FROM ACN 622306: ACFT WAS LEVELED OFF IN VMC AT 5000 FT MSL. QRC CHKLIST WAS RUN WITH NO RESULTS. 'TRIGGER PULL' WAS ACCOMPLISHED IN ACCORDANCE WITH THE CHKLIST. BOTH PLTS ATTEMPTED TO 'TRIGGER PULL,' GEAR HANDLE STILL WOULD NOT GO BEYOND 'OFF' POS. LANDED THE ACFT UNEVENTFULLY AT OKC APPROX 2000 LBS OVERWT (116200 LBS).

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.