Narrative:

Diverted to dfw due to reduced power on right engine. During en route climb from FL350 to FL390, the aircraft stopped climbing at FL356 and airspeed began decaying. At this time, the right engine EPR was noted pegged at maximum, while all other engine instruments were reading low. No EICAS messages were ever received. We requested and received FL350 where we could maintain approximately .74 mach. After reviewing the QRH and finding nothing matching our indications, it was suggested we might retard the right throttle and turn off the right engine electronic control to see if we would regain full power. However, prior to troubleshooting the problem ourselves, the captain elected to get a phone patch via dispatch to maintenance control. The patch was intermittent so another patch was obtained. After passing all engine readings to maintenance control, the reply was we had a pressure leak and would only have reduced power but otherwise a good engine. The captain decided to divert and recontacted dispatch with the results of the maintenance control communication. The decision was to divert into dfw which was along our route of flight. ATC handling went smoothly and we received direct and our request for descent to FL240. Approximately 5 mins after leveling at FL240, the right engine indications returned to normal and remained there for the duration of flight. A normal approach/landing was made at dfw.

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Original NASA ASRS Text

Title: B757-200 CREW HAD AN ENG THAT WOULD NOT PRODUCE RATED THRUST INFLT AT FL350.

Narrative: DIVERTED TO DFW DUE TO REDUCED PWR ON R ENG. DURING ENRTE CLB FROM FL350 TO FL390, THE ACFT STOPPED CLBING AT FL356 AND AIRSPD BEGAN DECAYING. AT THIS TIME, THE R ENG EPR WAS NOTED PEGGED AT MAX, WHILE ALL OTHER ENG INSTS WERE READING LOW. NO EICAS MESSAGES WERE EVER RECEIVED. WE REQUESTED AND RECEIVED FL350 WHERE WE COULD MAINTAIN APPROX .74 MACH. AFTER REVIEWING THE QRH AND FINDING NOTHING MATCHING OUR INDICATIONS, IT WAS SUGGESTED WE MIGHT RETARD THE R THROTTLE AND TURN OFF THE R ENG ELECTRONIC CTL TO SEE IF WE WOULD REGAIN FULL PWR. HOWEVER, PRIOR TO TROUBLESHOOTING THE PROB OURSELVES, THE CAPT ELECTED TO GET A PHONE PATCH VIA DISPATCH TO MAINT CTL. THE PATCH WAS INTERMITTENT SO ANOTHER PATCH WAS OBTAINED. AFTER PASSING ALL ENG READINGS TO MAINT CTL, THE REPLY WAS WE HAD A PRESSURE LEAK AND WOULD ONLY HAVE REDUCED PWR BUT OTHERWISE A GOOD ENG. THE CAPT DECIDED TO DIVERT AND RECONTACTED DISPATCH WITH THE RESULTS OF THE MAINT CTL COM. THE DECISION WAS TO DIVERT INTO DFW WHICH WAS ALONG OUR RTE OF FLT. ATC HANDLING WENT SMOOTHLY AND WE RECEIVED DIRECT AND OUR REQUEST FOR DSCNT TO FL240. APPROX 5 MINS AFTER LEVELING AT FL240, THE R ENG INDICATIONS RETURNED TO NORMAL AND REMAINED THERE FOR THE DURATION OF FLT. A NORMAL APCH/LNDG WAS MADE AT DFW.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.