Narrative:

On departure, gear would not retract, checked QRH for a checklist for problem, none was found. Check cockpit for gear pins. All 3 pins were accounted for. Recycled gear to see if possible sensor glitch, still would not retract. With handle down, we had 3 green down and locked lights. Returned to ZZZ for landing, normal, but overweight. Maintenance sum: flight was canceled. Aircraft was maintenance ferried to ZZZ1. Maintenance placed aircraft on jacks, cycled gear and found gear retraction normal. Found red unsafe light indication problem. Troubleshot to intermitting S3 switch on the left autothrottle switch pack. Right/right switch pack per maintenance manual. Cycled gear several times. All operations check and indications normal. Performed overweight landing inspection with no defects found. Aircraft okay for service.

Google
 

Original NASA ASRS Text

Title: A B737-300 ON TKOF CLB AT 100 FT WERE UNABLE TO RETRACT THE LNDG GEAR. RETURNED TO THE FIELD. CAUSED BY A FAILED THROTTLE MICROSWITCH.

Narrative: ON DEP, GEAR WOULD NOT RETRACT, CHKED QRH FOR A CHKLIST FOR PROB, NONE WAS FOUND. CHK COCKPIT FOR GEAR PINS. ALL 3 PINS WERE ACCOUNTED FOR. RECYCLED GEAR TO SEE IF POSSIBLE SENSOR GLITCH, STILL WOULD NOT RETRACT. WITH HANDLE DOWN, WE HAD 3 GREEN DOWN AND LOCKED LIGHTS. RETURNED TO ZZZ FOR LNDG, NORMAL, BUT OVERWT. MAINT SUM: FLT WAS CANCELED. ACFT WAS MAINT FERRIED TO ZZZ1. MAINT PLACED ACFT ON JACKS, CYCLED GEAR AND FOUND GEAR RETRACTION NORMAL. FOUND RED UNSAFE LIGHT INDICATION PROB. TROUBLESHOT TO INTERMITTING S3 SWITCH ON THE L AUTOTHROTTLE SWITCH PACK. R/R SWITCH PACK PER MAINT MANUAL. CYCLED GEAR SEVERAL TIMES. ALL OPS CHK AND INDICATIONS NORMAL. PERFORMED OVERWT LNDG INSPECTION WITH NO DEFECTS FOUND. ACFT OKAY FOR SVC.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.