Narrative:

Flying the ILS approach and at approximately 400 ft AGL, I felt a loud explosive sound beneath my cockpit seat. The concussion reverberated in the cockpit. Air conditioning flow into the fltdeck was reduced considerably. A check of all wind screens was made and found intact. All engine instruments were normal, on touchdown, idle reverse was selected (normal procedure for us) and both thrust reversers indicated normal deployment. Wheel braking commenced at 100 KIAS with normal deceleration. The aircraft exited the runway on a high speed taxiway at approximately 30 KTS. Upon clearing the runway the fltdeck began filling with smoke. The smoke was not electrical in nature. The cockpit door was opened to check for smoke in cabin. Flight attendant's 'chimmed' the fltdeck at the same instant. Smoke became thicker in the fltdeck as we rolled to a stop on parallel taxiway. Cockpit windows were both opened. At this time captain and myself made the decision to evacuate the aircraft. Captain ordered 'evacuation checklist.' I donned my oxygen mask and went speaker/hot microphone and began reading my evacuate/evacuation checklist. When checklists were complete and engines were shutdown, the smoke began subsiding. Captain and myself unstraped and helped passengers evacuate the aircraft. Fwd slides were deployed and all passenger '48 and crew 5' egressed the aircraft. I was ordered by captain to gather all passengers off the acfts left forward nose about 30 yards. Only possible injuries at the same time was a sprained ankle from one of the passengers. Callback conversation with reporter revealed the following information: the reporter stated the airplane was a fokker 100 and the cause of the explosive sound was the left pack heat exchanger rupture. The reporter said the pack heat exchangers are located beneath the cockpit floor. The reporter said the pack compartment was filled with hot engine bleed air mixing with oil from the air cycle machine causing the cockpit and cabin smoke. The reporter said the aircraft was evacuated on the ground with only one passenger incurring a twisted ankle.

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Original NASA ASRS Text

Title: A FOKKER 100 ON FINAL APCH AT 400 FT EXPERIENCES EXPLOSIVE SOUND BELOW COCKPIT SEATS ON GROUND, COCKPIT AND CABIN FILLED WITH SMOKE. SMOKE CAUSED BY RUPTURED LEFT PACK HEAD EXCHANGER.

Narrative: FLYING THE ILS APCH AND AT APPROX 400 FT AGL, I FELT A LOUD EXPLOSIVE SOUND BENEATH MY COCKPIT SEAT. THE CONCUSSION REVERBERATED IN THE COCKPIT. AIR CONDITIONING FLOW INTO THE FLTDECK WAS REDUCED CONSIDERABLY. A CHK OF ALL WIND SCREENS WAS MADE AND FOUND INTACT. ALL ENG INSTRUMENTS WERE NORMAL, ON TOUCHDOWN, IDLE REVERSE WAS SELECTED (NORMAL PROCEDURE FOR US) AND BOTH THRUST REVERSERS INDICATED NORMAL DEPLOYMENT. WHEEL BRAKING COMMENCED AT 100 KIAS WITH NORMAL DECELERATION. THE ACFT EXITED THE RWY ON A HIGH SPEED TXWY AT APPROX 30 KTS. UPON CLEARING THE RWY THE FLTDECK BEGAN FILLING WITH SMOKE. THE SMOKE WAS NOT ELECTRICAL IN NATURE. THE COCKPIT DOOR WAS OPENED TO CHK FOR SMOKE IN CABIN. FA'S 'CHIMMED' THE FLTDECK AT THE SAME INSTANT. SMOKE BECAME THICKER IN THE FLTDECK AS WE ROLLED TO A STOP ON PARALLEL TXWY. COCKPIT WINDOWS WERE BOTH OPENED. AT THIS TIME CAPT AND MYSELF MADE THE DECISION TO EVACUATE THE ACFT. CAPT ORDERED 'EVACUATION CHKLIST.' I DONNED MY OXYGEN MASK AND WENT SPEAKER/HOT MIC AND BEGAN READING MY EVAC CHKLIST. WHEN CHKLISTS WERE COMPLETE AND ENGS WERE SHUTDOWN, THE SMOKE BEGAN SUBSIDING. CAPT AND MYSELF UNSTRAPED AND HELPED PASSENGERS EVACUATE THE ACFT. FWD SLIDES WERE DEPLOYED AND ALL PAX '48 AND CREW 5' EGRESSED THE ACFT. I WAS ORDERED BY CAPT TO GATHER ALL PASSENGERS OFF THE ACFTS LEFT FORWARD NOSE ABOUT 30 YARDS. ONLY POSSIBLE INJURIES AT THE SAME TIME WAS A SPRAINED ANKLE FROM ONE OF THE PASSENGERS. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE AIRPLANE WAS A FOKKER 100 AND THE CAUSE OF THE EXPLOSIVE SOUND WAS THE LEFT PACK HEAT EXCHANGER RUPTURE. THE RPTR SAID THE PACK HEAT EXCHANGERS ARE LOCATED BENEATH THE COCKPIT FLOOR. THE RPTR SAID THE PACK COMPARTMENT WAS FILLED WITH HOT ENG BLEED AIR MIXING WITH OIL FROM THE AIR CYCLE MACHINE CAUSING THE COCKPIT AND CABIN SMOKE. THE RPTR SAID THE ACFT WAS EVACUATED ON THE GROUND WITH ONLY ONE PAX INCURRING A TWISTED ANKLE.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.