Narrative:

Shortly after takeoff, the captain called for gear up, and upon completion, the smoke master warning panel went on, and the bell chimed. The so silenced the bell and declared that there was smoke in the left portion of the main cargo deck. Shortly after that, the captain and I argued that we smelled smoke. I switched over to departure control as the captain called for smoke on the flight deck, and we donned air masks and goggles and established communications. We then declared an emergency and began a right turn for a right downwind for runway 28R at sfo. While the captain flew the approach to a level off height, I gave the controller our souls on board and fuel, the so worked on the completion of the emergency checklist, and the smoke began to clear. We continued the traffic pattern and landed on runway 28R without further incident. We taxied to parking and were followed by local fire auths. No further events occurred. Callback conversation with reporter revealed the following information: the reporter stated the cause of the smoke was an internal and external engine oil leak, allowing oil to enter the engine bleed ducts direct to the air conditioning packs. The reporter stated the engine was a general electric CFM56-502C and was replaced. The reporter said the national transportation safety board requested and removed the cockpit voice recorder and flight data recorder.

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Original NASA ASRS Text

Title: AN AIRBUS 300 ON CLBOUT AT FL200 DECLARED AN EMER AND DIVERTED DUE TO SMOKE AND FUMES IN THE COCKPIT AND CARGO MAIN DECK CAUSED BY #1 ENG INTERNAL AND EXTERNAL OIL LEAK.

Narrative: SHORTLY AFTER TKOF, THE CAPT CALLED FOR GEAR UP, AND UPON COMPLETION, THE SMOKE MASTER WARNING PANEL WENT ON, AND THE BELL CHIMED. THE SO SILENCED THE BELL AND DECLARED THAT THERE WAS SMOKE IN THE L PORTION OF THE MAIN CARGO DECK. SHORTLY AFTER THAT, THE CAPT AND I ARGUED THAT WE SMELLED SMOKE. I SWITCHED OVER TO DEP CTL AS THE CAPT CALLED FOR SMOKE ON THE FLT DECK, AND WE DONNED AIR MASKS AND GOGGLES AND ESTABLISHED COMS. WE THEN DECLARED AN EMER AND BEGAN A R TURN FOR A R DOWNWIND FOR RWY 28R AT SFO. WHILE THE CAPT FLEW THE APCH TO A LEVEL OFF HEIGHT, I GAVE THE CTLR OUR SOULS ON BOARD AND FUEL, THE SO WORKED ON THE COMPLETION OF THE EMER CHECKLIST, AND THE SMOKE BEGAN TO CLEAR. WE CONTINUED THE TFC PATTERN AND LANDED ON RWY 28R WITHOUT FURTHER INCIDENT. WE TAXIED TO PARKING AND WERE FOLLOWED BY LOCAL FIRE AUTHS. NO FURTHER EVENTS OCCURRED. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE CAUSE OF THE SMOKE WAS AN INTERNAL AND EXTERNAL ENG OIL LEAK, ALLOWING OIL TO ENTER THE ENG BLEED DUCTS DIRECT TO THE AIR CONDITIONING PACKS. THE RPTR STATED THE ENG WAS A GENERAL ELECTRIC CFM56-502C AND WAS REPLACED. THE RPTR SAID THE NATIONAL TRANSPORTATION SAFETY BOARD REQUESTED AND REMOVED THE COCKPIT VOICE RECORDER AND FLT DATA RECORDER.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.