Narrative:

Emergency due to faulty pressurization system. We had maintenance on our aircraft prior to gate departure on our right pack. It was placarded prior to leaving the gate. Just as we rotated on takeoff, we experienced a loud noise that at first I thought was a nose tire failure. Then I got a call from the flight attendant telling me they heard the noise and were getting smoke and fumes in the cabin. I told the first officer to turn off the left pack and the noise stopped, followed by the cabin clearing. I declared an emergency, got vectors to runway 31R, made an uneventful landing, and after having the fire chief check the exterior of the aircraft, returned to the gate and deplaned the passenger. I put an entry in the logbook and noted the pack problem and that it was not an overweight landing.

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Original NASA ASRS Text

Title: F100 CREW WAS DISPATCHED WITH THE R PACK INOP. THEY HAD A L PACK FAILURE AT TKOF ROTATION AT DFW.

Narrative: EMER DUE TO FAULTY PRESSURIZATION SYS. WE HAD MAINT ON OUR ACFT PRIOR TO GATE DEP ON OUR R PACK. IT WAS PLACARDED PRIOR TO LEAVING THE GATE. JUST AS WE ROTATED ON TKOF, WE EXPERIENCED A LOUD NOISE THAT AT FIRST I THOUGHT WAS A NOSE TIRE FAILURE. THEN I GOT A CALL FROM THE FLT ATTENDANT TELLING ME THEY HEARD THE NOISE AND WERE GETTING SMOKE AND FUMES IN THE CABIN. I TOLD THE FO TO TURN OFF THE L PACK AND THE NOISE STOPPED, FOLLOWED BY THE CABIN CLRING. I DECLARED AN EMER, GOT VECTORS TO RWY 31R, MADE AN UNEVENTFUL LNDG, AND AFTER HAVING THE FIRE CHIEF CHK THE EXTERIOR OF THE ACFT, RETURNED TO THE GATE AND DEPLANED THE PAX. I PUT AN ENTRY IN THE LOGBOOK AND NOTED THE PACK PROB AND THAT IT WAS NOT AN OVERWT LNDG.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.