Narrative:

Rudder trim used on takeoff at approximately 7000 ft MSL. Functioned normally. Tried retrimming at FL390, rudder trim was inoperative both directions. Contacted dispatch and maintenance control. Tried resetting rudder trim circuit breaker -- no effect. Changed altitude, no effect. VMC conditions entire flight. Dispatch and I determined flight could be conducted safely and we proceeded to phx. Tried rudder trim approximately 1 hour later, and functioned normally. No emergency was ever declared.

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Original NASA ASRS Text

Title: A LARGE TRANSPORT IN CRUISE AT FL390 EXPERIENCED RUDDER TRIM FAILURE BOTH L AND R. ON GND 1 HR LATER TRIM FUNCTION NORMAL. SUSPECT COLD SOAK ICING.

Narrative: RUDDER TRIM USED ON TKOF AT APPROX 7000 FT MSL. FUNCTIONED NORMALLY. TRIED RETRIMMING AT FL390, RUDDER TRIM WAS INOP BOTH DIRECTIONS. CONTACTED DISPATCH AND MAINT CTL. TRIED RESETTING RUDDER TRIM CIRCUIT BREAKER -- NO EFFECT. CHANGED ALT, NO EFFECT. VMC CONDITIONS ENTIRE FLT. DISPATCH AND I DETERMINED FLT COULD BE CONDUCTED SAFELY AND WE PROCEEDED TO PHX. TRIED RUDDER TRIM APPROX 1 HR LATER, AND FUNCTIONED NORMALLY. NO EMER WAS EVER DECLARED.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.