Narrative:

Approximately 1 1/2 hours after takeoff, we smelled a 'burning electrical' smell around row X to row a and notified captain. The flight engineer came back and the smell was stronger. She reported to the captain, who came back to check. All air conditioning recirculation fans and other electrical were turned off and captain made decision to return to hnl. He informed us to prepare for planned evacuate/evacuation. Passenger were briefed and our checklists completed prior to uneventful landing in hnl. Even with several electrical system turned off, smell of burning electrical was still very strong in cabin at time of landing. Callback conversation with reporter revealed the following information: the reporter stated that the electrical smell turned out to be the result of sloppy, careless maintenance. A mechanic must have put regular duct tape, instead of electrical tape, over the duct next to the air conditioning motor. The tape fried up like crisp bacon, thus the source of electrical fire fumes. Maintenance found the cause of the problem a whole day later, after taking the plane OTS overnight, and laying over the crew and the passenger. The cabin crew thoroughly prepared the cabin for evacuate/evacuation, including the choosing of 'helpers.' the captain kept everyone informed, and there was no panic.

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Original NASA ASRS Text

Title: FLT ATTENDANT RPT, DC10-10, HNL-SFO, ELECTRICAL FIRE SMELL AND FUMES, RETURN TO HNL. EMER EVAC PREPARATION. LANDED WITHOUT INCIDENT.

Narrative: APPROX 1 1/2 HRS AFTER TKOF, WE SMELLED A 'BURNING ELECTRICAL' SMELL AROUND ROW X TO ROW A AND NOTIFIED CAPT. THE FE CAME BACK AND THE SMELL WAS STRONGER. SHE RPTED TO THE CAPT, WHO CAME BACK TO CHK. ALL AIR CONDITIONING RECIRCULATION FANS AND OTHER ELECTRICAL WERE TURNED OFF AND CAPT MADE DECISION TO RETURN TO HNL. HE INFORMED US TO PREPARE FOR PLANNED EVAC. PAX WERE BRIEFED AND OUR CHKLISTS COMPLETED PRIOR TO UNEVENTFUL LNDG IN HNL. EVEN WITH SEVERAL ELECTRICAL SYS TURNED OFF, SMELL OF BURNING ELECTRICAL WAS STILL VERY STRONG IN CABIN AT TIME OF LNDG. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THAT THE ELECTRICAL SMELL TURNED OUT TO BE THE RESULT OF SLOPPY, CARELESS MAINT. A MECH MUST HAVE PUT REGULAR DUCT TAPE, INSTEAD OF ELECTRICAL TAPE, OVER THE DUCT NEXT TO THE AIR CONDITIONING MOTOR. THE TAPE FRIED UP LIKE CRISP BACON, THUS THE SOURCE OF ELECTRICAL FIRE FUMES. MAINT FOUND THE CAUSE OF THE PROB A WHOLE DAY LATER, AFTER TAKING THE PLANE OTS OVERNIGHT, AND LAYING OVER THE CREW AND THE PAX. THE CABIN CREW THOROUGHLY PREPARED THE CABIN FOR EVAC, INCLUDING THE CHOOSING OF 'HELPERS.' THE CAPT KEPT EVERYONE INFORMED, AND THERE WAS NO PANIC.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.