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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 425664 |
| Time | |
| Date | 199901 |
| Day | Thu |
| Local Time Of Day | 1801 To 2400 |
| Place | |
| Locale Reference | airport : zzz |
| State Reference | US |
| Altitude | agl bound lower : 0 agl bound upper : 0 |
| Environment | |
| Light | Night |
| Aircraft 1 | |
| Operator | common carrier : air carrier |
| Make Model Name | DC-9 10 |
| Flight Phase | ground : preflight |
| Flight Plan | IFR |
| Person 1 | |
| Affiliation | company : air carrier |
| Function | flight crew : captain oversight : pic |
| Experience | flight time last 90 days : 100 flight time total : 8500 flight time type : 3500 |
| ASRS Report | 425664 |
| Person 2 | |
| Affiliation | company : air carrier |
| Function | flight crew : first officer |
| Qualification | pilot : commercial |
| Events | |
| Anomaly | aircraft equipment problem : critical non adherence : published procedure non adherence : far |
| Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa other other : unspecified |
| Resolutory Action | none taken : detected after the fact |
| Consequence | Other |
| Supplementary | |
| Air Traffic Incident | other |
Narrative:
After pushback, while attempting to start #2 engine, after bringing the #2 fuel control lever to start, I noticed the ignition switch was still in the off position. I discontinued the #2 start and started #1 while #2 wound down to zero RPM. While reattempting to start #2, we experienced high egt and a significant 'torch.' it was then that I noticed that I never brought the #2 fuel control lever back to off, thus the #2 was never purged of fuel. The rampers signaled me with a flashlight of the problem and I closed the fuel control lever and immediately began to motor #2 to put the fire out. #2 egt got up to 480 degrees C. We shut #1 down and were towed back to the gate. The entire process took 10 mins from pushback to towing in. I can't think of any contributing factors other than the crew being tired.
Original NASA ASRS Text
Title: A DC9-10 ON #2 ENG START CREW EXPERIENCED TORCHING AND HIGH EXHAUST GAS TEMP DUE TO INCORRECT START PROCS.
Narrative: AFTER PUSHBACK, WHILE ATTEMPTING TO START #2 ENG, AFTER BRINGING THE #2 FUEL CTL LEVER TO START, I NOTICED THE IGNITION SWITCH WAS STILL IN THE OFF POS. I DISCONTINUED THE #2 START AND STARTED #1 WHILE #2 WOUND DOWN TO ZERO RPM. WHILE REATTEMPTING TO START #2, WE EXPERIENCED HIGH EGT AND A SIGNIFICANT 'TORCH.' IT WAS THEN THAT I NOTICED THAT I NEVER BROUGHT THE #2 FUEL CTL LEVER BACK TO OFF, THUS THE #2 WAS NEVER PURGED OF FUEL. THE RAMPERS SIGNALED ME WITH A FLASHLIGHT OF THE PROB AND I CLOSED THE FUEL CTL LEVER AND IMMEDIATELY BEGAN TO MOTOR #2 TO PUT THE FIRE OUT. #2 EGT GOT UP TO 480 DEGS C. WE SHUT #1 DOWN AND WERE TOWED BACK TO THE GATE. THE ENTIRE PROCESS TOOK 10 MINS FROM PUSHBACK TO TOWING IN. I CAN'T THINK OF ANY CONTRIBUTING FACTORS OTHER THAN THE CREW BEING TIRED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.