Narrative:

At origination we were delayed due to the valve problem in the #1 engine. It was fixed and logged in the book. Meaning we were signed off that it was fixed. We took off and felt no incident until we got a phone call from the captain stating that he shut down the #1 engine and that everything was ok, that we were 40 mi from mia and we did not need to prepare the cabin for an emergency landing. We landed with no incident and the same aircraft was repaired and as for the flight attendant crew I was on we went illegal to fly because too many hours on duty. The flight went out with no further incident.

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Original NASA ASRS Text

Title: FLT ATTENDANT RPT REGARDING B727 ENG VALVE PROB REQUIRING AN ENG SHUTDOWN AND A RETURN FOR MAINT. THIS RESULTED IN CABIN ATTENDANT ILLEGAL DUTY TIME.

Narrative: AT ORIGINATION WE WERE DELAYED DUE TO THE VALVE PROB IN THE #1 ENG. IT WAS FIXED AND LOGGED IN THE BOOK. MEANING WE WERE SIGNED OFF THAT IT WAS FIXED. WE TOOK OFF AND FELT NO INCIDENT UNTIL WE GOT A PHONE CALL FROM THE CAPT STATING THAT HE SHUT DOWN THE #1 ENG AND THAT EVERYTHING WAS OK, THAT WE WERE 40 MI FROM MIA AND WE DID NOT NEED TO PREPARE THE CABIN FOR AN EMER LNDG. WE LANDED WITH NO INCIDENT AND THE SAME ACFT WAS REPAIRED AND AS FOR THE FLT ATTENDANT CREW I WAS ON WE WENT ILLEGAL TO FLY BECAUSE TOO MANY HRS ON DUTY. THE FLT WENT OUT WITH NO FURTHER INCIDENT.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.