Narrative:

We started our initial descent into bos. Low oil pressure light illuminated. The oil pressure was in yellow arc. We then reduced power. Oil pressure continued to go down. We consulted checklist and performed engine failure in-flight checks and other required checks. Landing was uneventful. Mechanics later determined an o-ring failed on the #2 engine.

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Original NASA ASRS Text

Title: FLC OF A BEECH 1900 AIRLINER (BE02) SHUT DOWN THE R ENG DUE TO LOW OIL PRESSURE. EMER WAS DECLARED AND ATC GAVE PRIORITY HANDLING TO THEIR DEST WHERE THE FLT TERMINATED. THE CAUSE OF THE ENG PROB WAS DETERMINED TO BE A FAILED O-RING.

Narrative: WE STARTED OUR INITIAL DSCNT INTO BOS. LOW OIL PRESSURE LIGHT ILLUMINATED. THE OIL PRESSURE WAS IN YELLOW ARC. WE THEN REDUCED PWR. OIL PRESSURE CONTINUED TO GO DOWN. WE CONSULTED CHKLIST AND PERFORMED ENG FAILURE INFLT CHKS AND OTHER REQUIRED CHKS. LNDG WAS UNEVENTFUL. MECHS LATER DETERMINED AN O-RING FAILED ON THE #2 ENG.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.