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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 373026 |
| Time | |
| Date | 199706 |
| Day | Fri |
| Local Time Of Day | 1801 To 2400 |
| Place | |
| Locale Reference | atc facility : roa airport : va83 |
| State Reference | VA |
| Altitude | msl bound lower : 3000 msl bound upper : 3000 |
| Environment | |
| Flight Conditions | VMC |
| Light | Daylight |
| Aircraft 1 | |
| Controlling Facilities | tracon : roa tower : yul |
| Operator | general aviation : personal |
| Make Model Name | Cessna 150 |
| Operating Under FAR Part | Part 91 |
| Flight Phase | cruise other other |
| Flight Plan | None |
| Person 1 | |
| Affiliation | Other |
| Function | instruction : instructor |
| Qualification | other other : other pilot : instrument pilot : cfi pilot : commercial |
| Experience | flight time last 90 days : 40 flight time total : 300 flight time type : 245 |
| ASRS Report | 373026 |
| Person 2 | |
| Affiliation | Other |
| Function | instruction : trainee |
| Qualification | pilot : student |
| Events | |
| Anomaly | aircraft equipment problem : critical other anomaly other |
| Independent Detector | other flight crewa |
| Resolutory Action | flight crew : declared emergency other other |
| Consequence | Other |
| Supplementary | |
| Primary Problem | Aircraft |
Narrative:
I was conducting an instructional flight 11 NM northeast of roa at 3000 ft MSL when the engine started running extremely rough with moderate vibrations. I checked the fuel valve for the 'on' position, confirmed the mixture control was full rich, applied full carburetor heat and noted further power reduction. I then removed carburetor heat, checked each magneto position, then returned the ignition switch to the 'both' position. I set the transponder to 7700 and declared an emergency with roa departure. I informed roa departure that I intended to land at a private airstrip in fincastle, va. During the next several mins, I considered trying to return to roa but was uncertain if the engine would continue to hold partial power. In the interest of safety, I elected to stay with my original decision and land the airplane on the private airstrip which I had in sight. The approach and landing was without incident. An airplane mechanic turned the propeller through by hand several times and determined that a valve was stuck which shut down 1 of the 4 cylinders.
Original NASA ASRS Text
Title: THE ENG OF A C150 STARTED RUNNING VERY ROUGH CAUSING THE PLT INSTRUCTOR, ON A TRAINING FLT, TO DECLARE AN EMER AND DIVERT TO A NEARBY PVT AIRSTRIP. STUCK ENG VALVE WAS THE SUSPECTED CAUSE.
Narrative: I WAS CONDUCTING AN INSTRUCTIONAL FLT 11 NM NE OF ROA AT 3000 FT MSL WHEN THE ENG STARTED RUNNING EXTREMELY ROUGH WITH MODERATE VIBRATIONS. I CHKED THE FUEL VALVE FOR THE 'ON' POS, CONFIRMED THE MIXTURE CTL WAS FULL RICH, APPLIED FULL CARB HEAT AND NOTED FURTHER PWR REDUCTION. I THEN REMOVED CARB HEAT, CHKED EACH MAGNETO POS, THEN RETURNED THE IGNITION SWITCH TO THE 'BOTH' POS. I SET THE XPONDER TO 7700 AND DECLARED AN EMER WITH ROA DEP. I INFORMED ROA DEP THAT I INTENDED TO LAND AT A PVT AIRSTRIP IN FINCASTLE, VA. DURING THE NEXT SEVERAL MINS, I CONSIDERED TRYING TO RETURN TO ROA BUT WAS UNCERTAIN IF THE ENG WOULD CONTINUE TO HOLD PARTIAL PWR. IN THE INTEREST OF SAFETY, I ELECTED TO STAY WITH MY ORIGINAL DECISION AND LAND THE AIRPLANE ON THE PVT AIRSTRIP WHICH I HAD IN SIGHT. THE APCH AND LNDG WAS WITHOUT INCIDENT. AN AIRPLANE MECH TURNED THE PROP THROUGH BY HAND SEVERAL TIMES AND DETERMINED THAT A VALVE WAS STUCK WHICH SHUT DOWN 1 OF THE 4 CYLINDERS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.