Narrative:

At FL310 a throttle split was noticed. The split was about a 4 knob width apart. The left engine had been replaced that day. The flight diverted with an overweight landing in pit. The approach and landing were very routine. Callback conversation with reporter revealed the following information: maintenance communicated to this reporter via a company radio frequency that a 2 knob width throttle split was what they considered as maximum tolerance and they encouraged the crew to divert to pit. The B73S had been en route from phl to las. The reporter states that he was more comfortable with diverting than continuing. The split was so excessive that he wondered if it would keep on growing, and he didn't want to find out while in night flight over the rockies. The overweight landing required an overweight inspection. The reporter has only heard that the split was probably a result of a rigging problem and has heard nothing more since. After the landing the crew and passenger were able to make a quick airplane swap and continued the trip.

Google
 

Original NASA ASRS Text

Title: WHILE ENRTE AT FL310, A B73S FLC NOTICED A THROTTLE SPLIT OF ABOUT 4 KNOB WIDTHS WHEN MATCHING PWR SETTINGS. THE ENG HAD BEEN REPLACED EARLIER THAT DAY. THE FLT WAS DIVERTED FOR MAINT AND AN OVERWT LNDG WAS ACCOMPLISHED.

Narrative: AT FL310 A THROTTLE SPLIT WAS NOTICED. THE SPLIT WAS ABOUT A 4 KNOB WIDTH APART. THE L ENG HAD BEEN REPLACED THAT DAY. THE FLT DIVERTED WITH AN OVERWT LNDG IN PIT. THE APCH AND LNDG WERE VERY ROUTINE. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: MAINT COMMUNICATED TO THIS RPTR VIA A COMPANY RADIO FREQ THAT A 2 KNOB WIDTH THROTTLE SPLIT WAS WHAT THEY CONSIDERED AS MAX TOLERANCE AND THEY ENCOURAGED THE CREW TO DIVERT TO PIT. THE B73S HAD BEEN ENRTE FROM PHL TO LAS. THE RPTR STATES THAT HE WAS MORE COMFORTABLE WITH DIVERTING THAN CONTINUING. THE SPLIT WAS SO EXCESSIVE THAT HE WONDERED IF IT WOULD KEEP ON GROWING, AND HE DIDN'T WANT TO FIND OUT WHILE IN NIGHT FLT OVER THE ROCKIES. THE OVERWT LNDG REQUIRED AN OVERWT INSPECTION. THE RPTR HAS ONLY HEARD THAT THE SPLIT WAS PROBABLY A RESULT OF A RIGGING PROB AND HAS HEARD NOTHING MORE SINCE. AFTER THE LNDG THE CREW AND PAX WERE ABLE TO MAKE A QUICK AIRPLANE SWAP AND CONTINUED THE TRIP.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.