Narrative:

Lost cabin pressurization, cabin rate of climb indicator was pegged at plus 4000 ft. Asked ATC for lower 3 times then initiated emergency descent to 10000 ft. Never got a response from ATC. Deviated from FL200 to 10000 ft because of rapid depressurization. Callback conversation with reporter revealed the following: excessive cabin climb led flight crew to believe that they had lost part of the fuselage. An emergency descent was requested but clearance was given to similar sounding call sign ('xzz' instead of xyz'). Flight crew initiated further descent in VMC and in area of anticipated descent clearance. After the situation was under control at 10000 ft, the flight crew was unable to establish communication on last assigned frequency, so they went to approach. Flight was expedited. After landing it was discovered that a cargo door seal had blown leaving approximately a 4 inch gap. Maintenance remarked that this was a familiar problem. Reporter (monitoring pilot) stated that company's aviation psychologist followed-up on flight crew's reaction to the event -- extensive questionnaire involved. Supplemental information from acn 307828: could not notify ATC so squawked 7700.

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Original NASA ASRS Text

Title: RAPID CABIN PRESSURIZATION LOSS LED TO EMER DSCNT IN B737-200 WITHOUT CLRNC.

Narrative: LOST CABIN PRESSURIZATION, CABIN RATE OF CLB INDICATOR WAS PEGGED AT PLUS 4000 FT. ASKED ATC FOR LOWER 3 TIMES THEN INITIATED EMER DSCNT TO 10000 FT. NEVER GOT A RESPONSE FROM ATC. DEVIATED FROM FL200 TO 10000 FT BECAUSE OF RAPID DEPRESSURIZATION. CALLBACK CONVERSATION WITH REPORTER REVEALED THE FOLLOWING: EXCESSIVE CABIN CLB LED FLC TO BELIEVE THAT THEY HAD LOST PART OF THE FUSELAGE. AN EMER DSCNT WAS REQUESTED BUT CLRNC WAS GIVEN TO SIMILAR SOUNDING CALL SIGN ('XZZ' INSTEAD OF XYZ'). FLC INITIATED FURTHER DSCNT IN VMC AND IN AREA OF ANTICIPATED DSCNT CLRNC. AFTER THE SIT WAS UNDER CTL AT 10000 FT, THE FLC WAS UNABLE TO ESTABLISH COM ON LAST ASSIGNED FREQ, SO THEY WENT TO APCH. FLT WAS EXPEDITED. AFTER LNDG IT WAS DISCOVERED THAT A CARGO DOOR SEAL HAD BLOWN LEAVING APPROX A 4 INCH GAP. MAINT REMARKED THAT THIS WAS A FAMILIAR PROB. RPTR (MONITORING PLT) STATED THAT COMPANY'S AVIATION PSYCHOLOGIST FOLLOWED-UP ON FLC'S REACTION TO THE EVENT -- EXTENSIVE QUESTIONNAIRE INVOLVED. SUPPLEMENTAL INFORMATION FROM ACN 307828: COULD NOT NOTIFY ATC SO SQUAWKED 7700.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.