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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 303299 |
| Time | |
| Date | 199505 |
| Day | Tue |
| Local Time Of Day | 1201 To 1800 |
| Place | |
| Locale Reference | airport : acy |
| State Reference | NJ |
| Altitude | agl bound lower : 0 agl bound upper : 0 |
| Environment | |
| Flight Conditions | Marginal |
| Light | Daylight |
| Aircraft 1 | |
| Operator | general aviation : personal |
| Make Model Name | Any Unknown or Unlisted Aircraft Manufacturer |
| Operating Under FAR Part | Part 91 |
| Flight Phase | ground : preflight ground other : taxi |
| Flight Plan | IFR |
| Person 1 | |
| Affiliation | Other |
| Function | flight crew : single pilot |
| Qualification | pilot : instrument pilot : commercial |
| Experience | flight time last 90 days : 75 flight time total : 900 flight time type : 300 |
| ASRS Report | 303299 |
| Person 2 | |
| Affiliation | Other |
| Function | other personnel other personnel other |
| Qualification | other other : other |
| Events | |
| Anomaly | other anomaly other |
| Independent Detector | other other : unspecified |
| Resolutory Action | other |
| Consequence | Other |
| Supplementary | |
| Primary Problem | Flight Crew Human Performance |
| Air Traffic Incident | Pilot Deviation |
Narrative:
During a pouring rain, I was interrupted during my preflight while I was untying the left wing. After I spoke to the line-man, I continued my preflight, but failed to fully untie the aircraft. The tie-down was pulled from the ground and was noticed while I was taxiing. An a and P maintenance mechanic untied the tie-down and told me that the aircraft was fine. To prevent another occurrence, if interrupted during preflight, I start over and at the end of preflight I double- check the tie-downs.
Original NASA ASRS Text
Title: AN SMA PLT PULLED A TIE-DOWN OUT OF THE GND WHILE TAXIING AWAY.
Narrative: DURING A POURING RAIN, I WAS INTERRUPTED DURING MY PREFLT WHILE I WAS UNTYING THE L WING. AFTER I SPOKE TO THE LINE-MAN, I CONTINUED MY PREFLT, BUT FAILED TO FULLY UNTIE THE ACFT. THE TIE-DOWN WAS PULLED FROM THE GND AND WAS NOTICED WHILE I WAS TAXIING. AN A AND P MAINT MECH UNTIED THE TIE-DOWN AND TOLD ME THAT THE ACFT WAS FINE. TO PREVENT ANOTHER OCCURRENCE, IF INTERRUPTED DURING PREFLT, I START OVER AND AT THE END OF PREFLT I DOUBLE- CHK THE TIE-DOWNS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.