![]() |
37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
| Attributes | |
| ACN | 288960 |
| Time | |
| Date | 199411 |
| Day | Wed |
| Local Time Of Day | 0601 To 1200 |
| Place | |
| Locale Reference | airport : day |
| State Reference | OH |
| Altitude | agl bound lower : 500 agl bound upper : 500 |
| Environment | |
| Flight Conditions | IMC |
| Light | Daylight |
| Aircraft 1 | |
| Controlling Facilities | tracon : day |
| Operator | general aviation : instructional |
| Make Model Name | Any Unknown or Unlisted Aircraft Manufacturer |
| Operating Under FAR Part | Part 91 |
| Flight Phase | descent : approach landing : missed approach |
| Flight Plan | IFR |
| Person 1 | |
| Affiliation | Other |
| Function | instruction : instructor |
| Qualification | pilot : commercial pilot : cfi pilot : flight engineer pilot : instrument |
| Experience | flight time last 90 days : 200 flight time total : 950 flight time type : 400 |
| ASRS Report | 288969 |
| Person 2 | |
| Affiliation | Other |
| Function | flight crew : single pilot |
| Qualification | pilot : private |
| Events | |
| Anomaly | aircraft equipment problem : critical incursion : landing without clearance |
| Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
| Resolutory Action | flight crew : declared emergency other |
| Consequence | Other |
| Supplementary | |
| Primary Problem | Flight Crew Human Performance |
Narrative:
After completing an ASR approach into ffo and being cleared for the option, the missed approach was initiated. However, the engine was rough and producing only 2100 RPM. A decision was made to call tower and ask to return for an immediate landing due to a rough engine. We were cleared for the landing which was uneventful. It was raining at the time and after further inspection by a mechanic, water was found in the left magneto.
Original NASA ASRS Text
Title: SMA SEL PWR LOSS CAUSING PLT TO LAND AT ONCE DURING IFR APCH TRAINING.
Narrative: AFTER COMPLETING AN ASR APCH INTO FFO AND BEING CLRED FOR THE OPTION, THE MISSED APCH WAS INITIATED. HOWEVER, THE ENG WAS ROUGH AND PRODUCING ONLY 2100 RPM. A DECISION WAS MADE TO CALL TWR AND ASK TO RETURN FOR AN IMMEDIATE LNDG DUE TO A ROUGH ENG. WE WERE CLRED FOR THE LNDG WHICH WAS UNEVENTFUL. IT WAS RAINING AT THE TIME AND AFTER FURTHER INSPECTION BY A MECH, WATER WAS FOUND IN THE L MAGNETO.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.