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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 268246 |
| Time | |
| Date | 199404 |
| Day | Sun |
| Local Time Of Day | 1201 To 1800 |
| Place | |
| Locale Reference | atc facility : cmk airport : hpn |
| State Reference | NY |
| Altitude | msl bound lower : 7000 msl bound upper : 7000 |
| Environment | |
| Flight Conditions | IMC |
| Light | Daylight |
| Aircraft 1 | |
| Controlling Facilities | tower : lga |
| Operator | general aviation : personal |
| Make Model Name | Any Unknown or Unlisted Aircraft Manufacturer |
| Operating Under FAR Part | Part 91 |
| Flight Phase | cruise other other |
| Route In Use | enroute airway : n90 |
| Flight Plan | IFR |
| Person 1 | |
| Affiliation | Other |
| Function | flight crew : single pilot |
| Qualification | pilot : commercial pilot : instrument |
| Experience | flight time last 90 days : 11 flight time total : 950 flight time type : 100 |
| ASRS Report | 268246 |
| Person 2 | |
| Affiliation | government : faa |
| Function | controller : approach |
| Qualification | controller : radar |
| Events | |
| Anomaly | aircraft equipment problem : critical |
| Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
| Resolutory Action | flight crew : declared emergency none taken : unable other |
| Consequence | Other |
| Supplementary | |
| Primary Problem | Aircraft |
Narrative:
Flight on previous day (orh to teb) was VFR and uneventful. Return to orh was IFR. Run-up and climb were normal. After leveling at 7000 ft AGL, radios faded. A check of system revealed `altitude' circuit breaker had tripped. It was reset, radio contact was reestablished and controller reported radar transponder was not being received. Transponder was reset and worked. A short time later, circuit breaker tripped again and was reset. At this point, burning insulation was smelled in the cockpit by both pilot and passenger. The `altitude' circuit breaker was opened and landing at the nearest airport was requested. Pilot used own navigation and made ILS 16 approach at hpn without incident. The aircraft was taxied to a service facility. Alternator windings had fused and rotor was worn where brushes made contact. The alternator and voltage regulator were replaced, as was the master switch. However, a positive reading on the ammeter is still not present and maintenance is continuing to trouble- shoot the problem.
Original NASA ASRS Text
Title: ELECTRICAL SYS FAILURE DUE TO ALTERNATOR, VOLTAGE REGULATOR FAILURE.
Narrative: FLT ON PREVIOUS DAY (ORH TO TEB) WAS VFR AND UNEVENTFUL. RETURN TO ORH WAS IFR. RUN-UP AND CLB WERE NORMAL. AFTER LEVELING AT 7000 FT AGL, RADIOS FADED. A CHK OF SYS REVEALED `ALT' CIRCUIT BREAKER HAD TRIPPED. IT WAS RESET, RADIO CONTACT WAS REESTABLISHED AND CTLR RPTED RADAR XPONDER WAS NOT BEING RECEIVED. XPONDER WAS RESET AND WORKED. A SHORT TIME LATER, CIRCUIT BREAKER TRIPPED AGAIN AND WAS RESET. AT THIS POINT, BURNING INSULATION WAS SMELLED IN THE COCKPIT BY BOTH PLT AND PAX. THE `ALT' CIRCUIT BREAKER WAS OPENED AND LNDG AT THE NEAREST ARPT WAS REQUESTED. PLT USED OWN NAV AND MADE ILS 16 APCH AT HPN WITHOUT INCIDENT. THE ACFT WAS TAXIED TO A SVC FACILITY. ALTERNATOR WINDINGS HAD FUSED AND ROTOR WAS WORN WHERE BRUSHES MADE CONTACT. THE ALTERNATOR AND VOLTAGE REGULATOR WERE REPLACED, AS WAS THE MASTER SWITCH. HOWEVER, A POSITIVE READING ON THE AMMETER IS STILL NOT PRESENT AND MAINT IS CONTINUING TO TROUBLE- SHOOT THE PROB.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.