Narrative:

I was captain of medium large transport non stop lax-bwi. First officer made the takeoff. At approximately 1000 ft MSL, while I was switching to departure control, I felt the aircraft yaw. At first I thought it was wake turbulence, then I checked the engine instruments (normal), then I checked the rudder trim. I saw the rudder trim indicator moving past 9 units right trim. I grabbed the rudder trim control knob and commanded the rudder back to neutral. The rudder responded and went back to neutral. The first officer hand flew the aircraft to FL230 where we engaged the autoplt and pulled the rudder trim control circuit breaker. No further problems were noted and we continued to bwi and wrote up the rudder trim. Our aircraft was an originator in lax. I performed a rudder trim check prior to engine start and a flight control check prior to takeoff. Both checks were normal in all respects. No rudder trim knob sticking was noted. No rudder trim inputs were made by either pilot prior to the trim running away. I do not believe this problem was caused by a sticking knob. I wonder if this is in any way related to the lga accident. I know most of us flying this aircraft would prefer the old mechanical rudder trim system that is on the medium large transport.

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Original NASA ASRS Text

Title: AN MLG EXPERIENCES A RUNAWAY RUDDER TRIM DURING INITIAL CLB.

Narrative: I WAS CAPT OF MLG NON STOP LAX-BWI. FO MADE THE TKOF. AT APPROX 1000 FT MSL, WHILE I WAS SWITCHING TO DEP CTL, I FELT THE ACFT YAW. AT FIRST I THOUGHT IT WAS WAKE TURB, THEN I CHKED THE ENG INSTS (NORMAL), THEN I CHKED THE RUDDER TRIM. I SAW THE RUDDER TRIM INDICATOR MOVING PAST 9 UNITS R TRIM. I GRABBED THE RUDDER TRIM CTL KNOB AND COMMANDED THE RUDDER BACK TO NEUTRAL. THE RUDDER RESPONDED AND WENT BACK TO NEUTRAL. THE FO HAND FLEW THE ACFT TO FL230 WHERE WE ENGAGED THE AUTOPLT AND PULLED THE RUDDER TRIM CTL CIRCUIT BREAKER. NO FURTHER PROBS WERE NOTED AND WE CONTINUED TO BWI AND WROTE UP THE RUDDER TRIM. OUR ACFT WAS AN ORIGINATOR IN LAX. I PERFORMED A RUDDER TRIM CHK PRIOR TO ENG START AND A FLT CTL CHK PRIOR TO TKOF. BOTH CHKS WERE NORMAL IN ALL RESPECTS. NO RUDDER TRIM KNOB STICKING WAS NOTED. NO RUDDER TRIM INPUTS WERE MADE BY EITHER PLT PRIOR TO THE TRIM RUNNING AWAY. I DO NOT BELIEVE THIS PROB WAS CAUSED BY A STICKING KNOB. I WONDER IF THIS IS IN ANY WAY RELATED TO THE LGA ACCIDENT. I KNOW MOST OF US FLYING THIS ACFT WOULD PREFER THE OLD MECHANICAL RUDDER TRIM SYS THAT IS ON THE MLG.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.