Narrative:

I was flying the aircraft when the incident occurred. At liftoff the aircraft experienced an over pressurization. While the captain and so handled the situation, I flew the airplane. We did not go above 10000 ft. We returned to boston flying an ILS to runway 4R. 4 passenger received treatment from paramedics when we blocked in. Supplemental information from acn 194866: shortly after the positive rate callout, my ears started popping. I looked at the so's panel and noticed the cabin rate of change indicator was pegged at 2000 FPM of descent. The automatic fail light and standby light were on. Cabin altitude was 5000 ft, and cabin psid was 9.3 psid. The so switched to manual dc. We still were unable to control the cabin pressurization.

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Original NASA ASRS Text

Title: ACR LGT PRESSURIZATION PROBLEM DURING CLB OUT FROM BOS. RETURN LAND.

Narrative: I WAS FLYING THE ACFT WHEN THE INCIDENT OCCURRED. AT LIFTOFF THE ACFT EXPERIENCED AN OVER PRESSURIZATION. WHILE THE CAPT AND SO HANDLED THE SITUATION, I FLEW THE AIRPLANE. WE DID NOT GO ABOVE 10000 FT. WE RETURNED TO BOSTON FLYING AN ILS TO RWY 4R. 4 PAX RECEIVED TREATMENT FROM PARAMEDICS WHEN WE BLOCKED IN. SUPPLEMENTAL INFO FROM ACN 194866: SHORTLY AFTER THE POSITIVE RATE CALLOUT, MY EARS STARTED POPPING. I LOOKED AT THE SO'S PANEL AND NOTICED THE CABIN RATE OF CHANGE INDICATOR WAS PEGGED AT 2000 FPM OF DSCNT. THE AUTO FAIL LIGHT AND STANDBY LIGHT WERE ON. CABIN ALT WAS 5000 FT, AND CABIN PSID WAS 9.3 PSID. THE SO SWITCHED TO MANUAL DC. WE STILL WERE UNABLE TO CTL THE CABIN PRESSURIZATION.

Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.