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| Attributes | |
| ACN | 1725168 |
| Time | |
| Date | 202002 |
| Local Time Of Day | 1801-2400 |
| Place | |
| Locale Reference | ZZZ.Airport |
| State Reference | US |
| Aircraft 1 | |
| Make Model Name | A320 |
| Operating Under FAR Part | Part 121 |
| Flight Phase | Climb |
| Flight Plan | IFR |
| Person 1 | |
| Function | Captain Pilot Flying |
| Qualification | Flight Crew Instrument Flight Crew Air Transport Pilot (ATP) Flight Crew Multiengine |
| Events | |
| Anomaly | Aircraft Equipment Problem Less Severe Deviation - Procedural Maintenance Deviation - Procedural Weight And Balance Flight Deck / Cabin / Aircraft Event Smoke / Fire / Fumes / Odor |
Narrative:
After takeoff from ZZZ we noticed an unusual odor like wet socks as we continued the climb the odor never dissipated. We leveled off at FL280; I gave controls of aircraft to [the] first officer and called dispatch/maintenance. I was told there was a previous write up; but were not able to duplicate. After consulting with both it was determined to return to ZZZ. An overweight landing was performed approximately 3;400 lbs over and touchdown was less than 200 FPM. Upon reaching gate maintenance came aboard and at that point I was informed for the first time that apparently some blades were changed not sure if maybe some residual oil/grease might have been left and got into the system? I was surprised that maintenance control center didn't know that maintenance had been done on that day.
Original NASA ASRS Text
Title: A320 Captain reported an air return due to a fume event during initial climb.
Narrative: After takeoff from ZZZ we noticed an unusual odor like wet socks as we continued the climb the odor never dissipated. We leveled off at FL280; I gave controls of aircraft to [the] First Officer and called Dispatch/Maintenance. I was told there was a previous write up; but were not able to duplicate. After consulting with both it was determined to return to ZZZ. An overweight landing was performed approximately 3;400 lbs over and touchdown was less than 200 FPM. Upon reaching gate Maintenance came aboard and at that point I was informed for the first time that apparently some blades were changed not sure if maybe some residual oil/grease might have been left and got into the system? I was surprised that Maintenance Control Center didn't know that maintenance had been done on that day.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.