Narrative:

Climbing through fl 210 we got a cabin altitude warning and horn and passenger oxygen masks deployment. We immediately donned our oxygen masks and established communication. We then notified ATC of our problem and leveled off at fl 220. The captain ran the qrc and QRH while I flew the aircraft. We noticed the cabin altitude was stable at 15;000 feet; although this was neither an explosive or rapid decompression we clearly had a pressurization problem with only partial pressurization; so we [advised ATC] and descended to 10;000 feet. We then requested a turn back to ZZZ and finished our checklist and requested overweight landing data as we would be 800 pounds over max landing weight. We did a normal flaps 30 landing followed by normal brake application. After turning off the runway we had the [arff personnel] do an inspection of our landing gear for any hot brakes. After getting the all clear we proceeded to the gate and deplaned. The maintenance technician then advised us of a failed one way check valve in the external ground air receptacle which was the cause.

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Original NASA ASRS Text

Title: B737 flight crew reported a pressurization issue led to a return to the departure airport.

Narrative: Climbing through FL 210 we got a cabin altitude warning and horn and passenger oxygen masks deployment. We immediately donned our oxygen masks and established communication. We then notified ATC of our problem and leveled off at FL 220. The captain ran the QRC and QRH while I flew the aircraft. We noticed the cabin altitude was stable at 15;000 feet; although this was neither an explosive or rapid decompression we clearly had a pressurization problem with only partial pressurization; so we [advised ATC] and descended to 10;000 feet. We then requested a turn back to ZZZ and finished our checklist and requested overweight landing data as we would be 800 pounds over max landing weight. We did a normal flaps 30 landing followed by normal brake application. After turning off the runway we had the [ARFF personnel] do an inspection of our landing gear for any hot brakes. After getting the all clear we proceeded to the gate and deplaned. The maintenance technician then advised us of a failed one way check valve in the external ground air receptacle which was the cause.

Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.