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37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
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| Attributes | |
| ACN | 1499393 |
| Time | |
| Date | 201711 |
| Local Time Of Day | 0601-1200 |
| Place | |
| Locale Reference | ZZZ.Airport |
| State Reference | US |
| Environment | |
| Flight Conditions | VMC |
| Light | Daylight |
| Aircraft 1 | |
| Make Model Name | Caravan 208B |
| Operating Under FAR Part | Part 135 |
| Flight Phase | Takeoff |
| Flight Plan | VFR |
| Component | |
| Aircraft Component | Turbine Engine |
| Person 1 | |
| Function | Captain Pilot Flying |
| Qualification | Flight Crew Commercial Flight Crew Instrument Flight Crew Flight Instructor |
| Experience | Flight Crew Last 90 Days 200 Flight Crew Total 1400 Flight Crew Type 1000 |
| Events | |
| Anomaly | Aircraft Equipment Problem Critical |
Narrative:
I briefed my departure as we taxied out- to include a short field takeoff. I applied 2000 ft-lbs (company takeoff limit); saw gauges in the green; and released the brakes. It seemed to take a little longer than normal to rotate; but we had nine passengers so it didn't seem too abnormal. About 8-10 feet off the ground; I sensed a lack of power and felt slow. I glanced at the engine gauges and noticed right away that torque was at 1400 ft-lbs and decreasing. My initial thought was that one of us had unintentionally knocked the power lever back; so I attempted to add more power; and only watched the power continue to decrease. I said to the first officer; 'I just lost my power; I'm putting it back down.' I pulled power back to idle; landed on the remaining runway; put it in beta; applied brakes; and stopped before the end of the runway. Immediately after touching back down; the cockpit filled with the smell of jet fuel. I made the decision since we still had power and were not experiencing a fire to taxi back to parking and shut the engine down. I called the mechanic and he drove over to assess the problem. After hours of trouble-shooting; it was found that an o-ring in the fuel manifold was punctured on installation. We were the first crew to fly the aircraft after the fuel nozzles had been replaced; and that's when it occurred.
Original NASA ASRS Text
Title: C208B Captain reported rejecting the takeoff shortly after liftoff when he experienced a loss of power related to a leaking o-ring in the fuel manifold.
Narrative: I briefed my departure as we taxied out- to include a short field takeoff. I applied 2000 ft-lbs (company takeoff limit); saw gauges in the green; and released the brakes. It seemed to take a little longer than normal to rotate; but we had nine passengers so it didn't seem too abnormal. About 8-10 feet off the ground; I sensed a lack of power and felt slow. I glanced at the engine gauges and noticed right away that torque was at 1400 ft-lbs and decreasing. My initial thought was that one of us had unintentionally knocked the power lever back; so I attempted to add more power; and only watched the power continue to decrease. I said to the FO; 'I just lost my power; I'm putting it back down.' I pulled power back to idle; landed on the remaining runway; put it in beta; applied brakes; and stopped before the end of the runway. Immediately after touching back down; the cockpit filled with the smell of jet fuel. I made the decision since we still had power and were not experiencing a fire to taxi back to parking and shut the engine down. I called the mechanic and he drove over to assess the problem. After hours of trouble-shooting; it was found that an o-ring in the fuel manifold was punctured on installation. We were the first crew to fly the aircraft after the fuel nozzles had been replaced; and that's when it occurred.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.