![]() |
37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
| Attributes | |
| ACN | 1383939 |
| Time | |
| Date | 201608 |
| Local Time Of Day | 0601-1200 |
| Place | |
| Locale Reference | ZZZ.TRACON |
| State Reference | US |
| Environment | |
| Flight Conditions | VMC |
| Light | Daylight |
| Aircraft 1 | |
| Make Model Name | M-20 K (231) / Encore |
| Operating Under FAR Part | Part 91 |
| Flight Phase | Cruise |
| Flight Plan | VFR |
| Component | |
| Aircraft Component | Engine |
| Person 1 | |
| Function | Pilot Flying Single Pilot |
| Qualification | Flight Crew Private |
| Experience | Flight Crew Last 90 Days 73 Flight Crew Total 767 Flight Crew Type 3 |
| Events | |
| Anomaly | Aircraft Equipment Problem Critical Ground Event / Encounter Ground Strike - Aircraft |
Narrative:
During a test flight of a newly purchased airplane within 5 to 7 minutes after takeoff I experienced two quick pops from the engine. Within 3 seconds of engine popping; the engine quit. I turned on the low boost pump and switched fuel tanks. The engine was still popping and making 20% power to 0% power. I held the high boost pump to the on position and the engine would make a bit more power; however was still losing altitude. After reaching 800 feet AGL picked a suitable off field landing. Set the airplane up with flaps/trim and gear down and committed to my off field landing. After coming to a stop and exiting the airplane; noticed a blue streak of liquid down the left-side of fuselage. Raised oil fill door on top of engine cowling and noticed strong fuel odor. Upon further inspection; found a 1/4 inch fuel line disconnected on fuel system.
Original NASA ASRS Text
Title: M20K pilot reported landing in a field after the engine quit in flight. Inspection on the ground revealed a fuel line had become disconnected.
Narrative: During a test flight of a newly purchased airplane within 5 to 7 minutes after takeoff I experienced two quick pops from the engine. Within 3 seconds of engine popping; the engine quit. I turned on the low boost pump and switched fuel tanks. The engine was still popping and making 20% power to 0% power. I held the high boost pump to the on position and the engine would make a bit more power; however was still losing altitude. After reaching 800 feet AGL picked a suitable off field landing. Set the airplane up with flaps/trim and gear down and committed to my off field landing. After coming to a stop and exiting the airplane; noticed a blue streak of liquid down the left-side of fuselage. Raised oil fill door on top of engine cowling and noticed strong fuel odor. Upon further inspection; found a 1/4 inch fuel line disconnected on fuel system.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.