Narrative:

After takeoff (approximately 400' AGL), left torque gauge began giving very erratic readings. Flight crew attempted to assess problem and decided an engine shutdown and return for landing was in best interest of safety of flight. Notified fsm tower of our intentions (we did declare an emergency). They had equipment standing by for us. After caging left engine, we called for and completed all normal/abnormal/emergency checklists as appropriate. We entered a left downwind and executed smooth landing. Maintenance check showed a faulty np sensor was giving us erroneous torque readings. Maximum torque is 108%. We made a reduced power takeoff (94%). Gauge was fluctuating between 40-120%.

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Original NASA ASRS Text

Title: FLT CREW OF MDT HAD ERRATIC TORQUE READINGS AFTER TKOF. RETURNED, LANDED.

Narrative: AFTER TKOF (APPROX 400' AGL), LEFT TORQUE GAUGE BEGAN GIVING VERY ERRATIC READINGS. FLT CREW ATTEMPTED TO ASSESS PROB AND DECIDED AN ENG SHUTDOWN AND RETURN FOR LNDG WAS IN BEST INTEREST OF SAFETY OF FLT. NOTIFIED FSM TWR OF OUR INTENTIONS (WE DID DECLARE AN EMER). THEY HAD EQUIP STANDING BY FOR US. AFTER CAGING LEFT ENG, WE CALLED FOR AND COMPLETED ALL NORMAL/ABNORMAL/EMER CHKLISTS AS APPROPRIATE. WE ENTERED A LEFT DOWNWIND AND EXECUTED SMOOTH LNDG. MAINT CHK SHOWED A FAULTY NP SENSOR WAS GIVING US ERRONEOUS TORQUE READINGS. MAX TORQUE IS 108%. WE MADE A REDUCED PWR TKOF (94%). GAUGE WAS FLUCTUATING BTWN 40-120%.

Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.